HomeMy WebLinkAboutBIRCHWOOD LOOP S12343 Onsite File
Birchwood Loop
#512343
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GARNESS ENGINEERING GROUP, Ltd AG'"a..,C'Yir
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CIVIL&ENVIRONMENTAL ENGINEERS Dealer
November 1, 2017 (REVISED)
S4 Group, LLC
124 East 7th Avenue
Anchorage, Alaska 99501
Phone: (907) 306-8104
Ref: Well and Septic Reserve Areas for T15N, R1 W, Section 19, Lot 4 (Birchwood Loop Subdivision, Case# S12343)
The following is a list of the test hole numbers, total depths, the groundwater levels, the percolation rate, and the minimum
square footage for septic reserve areas for the proposed subdivision:
Pro- Test Total 5/11/2017 G.W.M. **Depth to Percolation Minimum Septic
posed Hole # Depth (unless noted Impermeabl Rate Reserve Area
Lot # otherwise) e Soils
LOT 1 GEG-TH#1 13' 5' 10' - 120 min./inch ATS only
LOT 1 *C.W.-TH#1 16' 6' 7' ***26.7 min./inch 16,000 sq.ft.
•
LOT 1 GEG-TH#2 12' 3.75' 10' 10.9 min./inch 12,000 sq.ft.
LOT 1 *C.W.-TH#2A 15' 12' (11/20/07) 7' >120 min./inch Not suitable
LOT 1 *C.W.-TH#2B 14' 6.5' 8' ***34.3 min./inch 16,000 sq.ft.
-
LOT 2 *C.W.-TH#3 15' 8' 4' _ ***30 min./inch 16,000 sq.ft.
LOT 2 GEG-TH#3 12' 2' 6'-7' >120 min./inch Not suitable
•
LOT 2 GEG-TH#4 13.5' 7.5' N/A 4 min./inch 10,000 sq.ft
•
LOT 2 *C.W.-TH#4B 14' DRY 13' <1 min./inch 10,000 sq.ft.
LOT 2 *C.W.-TH#4C ****N.L. 5.5' ****N.L. ****N.L. ****N.L.
LOT 2 *C.W.-TH#4D 14' 10.75' 13' <1 min./inch 10,000 sq.ft.
LOT 3 TH#1 (2002) 13' DRY(10/11/00) N/A 20 min./inch 14,000 sq.ft.
LOT 3 TH#2 (2002) 14' 12.5'(10/11/00) N/A _• 26 min./inch 16,000 sq.ft.
LOT 3 *****D.D.-TH#1 17' 11'(5/10/1992) N/A No Perk N/A
LOT 3 *****D.D.-TH#2 17' 14'(5/10/1992) N/A 44 min./inch 16,000 sq.ft
LOT 4 *C.W.-TH#4 16' 12' N/A 40 min./inch 16,000 sq.ft.
LOT 4 GEG-TH#5 13' 11' N/A 9.2 min/inch 12,000 sq.ft.
LOT 5 *C.W.-TH#5 5' 2'(11/20/07) 2' No Perk Not suitable
LOT 5 GEG-TH#6 12.5' 3' 7' ▪ 48 min/inch 16,000 sq.ft.
LOT 6 *C.W.-TH#6 12' 3'(11/20/07) 4' No Perk Not suitable
LOT 6 GEG-TH#7 12.5' 1.5' 10' • 34.3 min/inch 16,000 sq.ft.
LOT 6 *C.W.-TH#7 11' No record 6' 21.8 min/inch 14,000 sq.ft.
LOT 6 GEG-TH#8 12' 2' _ 7' 20 min./inch 14,000 sq.ft.
*C.W. = Christopher Wood, P.E. — See soil logs
**To visually rated impermeable soils (soil>120 minutes/inch)
***Re-benched Christopher Wood, P.E. test holes to confirm percolation rates. C.W. initially had >120 minute/inch
percolation rates on these holes. It is possible these perk benches were improperly set-up or may have been influenced by
heavy precipitation and/or freezing conditions. GEG found suitable percolation rates next to these test holes. In short, soil
may vary significantly throughout area.
****N.L. = No Log — Soil log could not be found for this test hole. GWM tube was found by GEG in the general test hole
location identified by C.W. and assumed to be C.W.-TH#4C.
3701 East Tudor Road, Suite 101 *Anchorage,Alaska 99507-1259
Phone: (907)337-6179*Fax: (907)338-3246*Website: www.garnessengineering.com
Page 2 of 4
"""D.D. — David Dayton. P.E. — See soils logs. Locations of the test hole per 2000 David Dayton design and 2002 GEG
record drawings
GEG = Garness Engineering Group, Ltd.
Well and Septic Reserve Site Plan:
The owner is proposing to subdivide the eighteen (18) acre tract of land into six (6) lots. Attached is a site plan which
shows the proposed lot lines for subdividing the property, as well as the proposed/existing wells on the subject property,
and the proposed septic reserve areas. In 2007, Christopher Woods (C.W.). P.E. performed multiple test holes for the
owner for the purpose of subdividing the parcel. Mr. Woods provided the owner a copy of the signed soils logs which can
no longer be located. The owner has made several attempts to get signed original soils logs from Mr. Woods, but has not
been able to reach him. C.W.'s soils logs show the percolation rate, however, they do not show 7-day groundwater
monitoring. We have provided a copy of these test holes for informational purposes only. C.W. also provided a sketch
drawing (see Exhibit A) of the test hole locations which is attached. In December of 2016, the owner hired Garness
Engineering Group, Ltd (GEG) to perform additional test holes on the property for the purpose of subdividing the parcel.
Prior to excavating these test holes, S4 Group, Ltd. staked all the new GEG proposed test hole locations and surveyed in
all C.W.'s test holes that were shown on his sketch drawing, except for C.W.-TH#5 & C.W.-TH#8. GEG performed eight
(8) new test holes and also re-benched three (3) of C.W.'s test holes (C.W.-TH#1, C.W.-TH#2B, & C.W.-TH#3) and
performed new percolation tests. In addition to this, GEG performed 7-day groundwater monitoring (gwm) on all new test
holes and all C.W. monitoring tubes except for CW-TH#5, CW-TH#6, & CW-TH#7 which could not be found. In addition to
these test holes, there are four(4) other test holes on the property. Two (2) test holes were performed by GEG in 2002
and two (2) test holes were performed by David Dayton, P.E. (D.D.) in 2000. These test hole locations are shown on the
attached site plan and the locations are based upon a design done by D.D. and a record drawing done by GEG. The
following is a brief explanation of the soils and groundwater conditions for each proposed lot:
Proposed Lot 1
A total of five (5) test holes have been excavated within the proposed Lot 1 boundary. As can been seen on the attached site
plan, there are two (2)test holes within the proposed septic reserve area (GEG-TH#2 and C.W.-TH#1). The percolation rate
for the GEG test hole (GEG-TH#2) was 10.9 minutes/inch and the percolation rate for C.W.-TH#1 was 26.7 minutes/inch.
We are proposing to use the average percolation rate for these two test holes of 18.8 minutes/inch, which dictates a
minimum septic reserve area of 14,000 sq.ft. As can been seen from the topography on the site plan, the average slope
within the septic reserve area ranges from 7 to 10 percent, running approximately south to north. A proposed well has been
shown on the site plan.
Proposed Lot 2
A total of six (5) test holes have been excavated within the proposed lot boundary. As can been seen on the attached site
plan, there are four(4) test holes within the proposed septic reserve area or immediately adjacent to it(GEG-TH#3; C.W.-
TH#4B; C.W.-TH#4C; and C.W.-TH#4D). The percolation rates for these four test holes ranged from <1 to 4 minutes/inch,
which dictates a minimum septic reserve area of 10,000 sq.ft. As can been seen from the topography on the site, the
average slope within the septic reserve area ranges from 5 to 7 percent, running approximately south/southeast to
north/northwest. A proposed well has been shown on the site plan.
Proposed Lot 3
A total of four(4)test holes have been excavated within the proposed lot boundary. As can been seen on the attached site
plan, there is one (1)test hole within the proposed septic reserve area, TH#2 (logged by GEG in 2002). The percolation rate
for this test hole was 26 minutes/inch, which dictates a minimum septic reserve area of 16,000 sq.ft. As can been seen from
the topography on the site plan, the average slope within the septic reserve area ranges from 10 to 15 percent, running
approximately southeast to northwest. There is an existing septic tank and drainfield on the property, but it is not approved.
The owner of the property does not want to use this septic system and plans on completely abandoning the system. There
is an existing private well located on this property that will be used to serve a future residence.
3701 East Tudor Road, Suite 101 *Anchorage,Alaska 99507-1259
Phone: (907)337-6179*Fax: (907)338-3246*Website:www.garnessengineering.com
Page 3 of 4
Proposed Lot 4
A total of two (2) test holes have been excavated within the proposed lot boundary. As can been seen on the attached site
plan, there are two (2) test holes within the proposed septic reserve area, GEG-TH#5 & C.W.-TH#4. The percolation rate
for the GEG test hole was 9.2 minutes/inch and Christopher Wood's percolation rate was 40 minutes/inch. We are
proposing to use the average percolation rate for these two test holes of 24.5 minutes/inch, which dictates a minimum
septic reserve area of 16,000 sq.ft. As can been seen from the topography on the site plan, the average slope within the
septic reserve area ranges from 15 to 20 percent, running approximately southeast to northwest. There is an old Quonset
hut type structure on this lot that is proposed (by the owner) to be removed. A proposed well has been shown on the site
plan.
Proposed Lot 5
A total two (2) test holes have been excavated within the proposed lot boundary. As can been seen on the attached site
plan, GEG-TH#6 is within the proposed septic reserve area. The percolation rate for this test hole was 34.3 minutes/inch,
which dictates a minimum septic reserve area of 16,000 sq.ft. As can been seen from the topography on the site plan, the
average slope within the septic reserve area ranges from 15 to 20 percent, running approximately southeast to northwest.
There is an old Quonset hut type structure on this lot that is proposed (by the owner) to be removed. A proposed well has
been shown on the site plan.
Proposed Lot 6
A total of four(4) test holes have been excavated within the proposed lot boundary. As can been seen on the attached
site plan, there are two (2) test holes within the proposed septic reserve area (GEG-TH#8 & C.W.-TH#7). The percolation
rate for the GEG test hole was 20 minutes/inch and Christopher Wood's percolation rate was 21.8 minutes/inch. Based
upon these percolation rates, the minimum septic reserve area is 14,000 sq.ft. As can been seen from the topography on
the site plan, the average slope within the septic reserve area ranges from 10 to 15 percent, running approximately
southeast to northwest. A proposed well has been shown on the site plan. Due to high spring groundwater levels, an ERS
system will be required for this property. We have requested a septic permit be issued for the property in the area of this
proposed lot. With the issuance of a septic permit, this will insure that this lot is developable prior to the completion of the
subdivision process.
Conclusion for Septic Reserve Areas
Based upon the aforementioned conditions, it is reasonable to believe that the proposed lots will support onsite septic
systems; however, due to the presence of some impermeable soils (C.W. percolation tests) and shallow groundwater,
many (if not all) of the proposed lots will likely require a Cat II (or higher) advanced wastewater treatment system and an
ERS system will be required for Lot 6.
Water Availability
We have performed records research on some of the surrounding properties and have attached the well logs and other
well information. The attached is a site plan shows the approximate location of the existing wells on adjacent properties.
The following is a summary of our findings regarding these wells:
• There is a well located on Birchwood S/D; Lot 3 which serves Grace Brethren Church. Based upon the well log,
the well is 124 feet deep, had a static water level at 20 feet, and is cased to 54 feet. Based upon the well log, the
well flow production was found to be 5 gpm (300 gph) in April of 1985.
• There is a well located on Birchwood S/D; Tract A which serves a private residence. Based upon the 1990 Health
Authority Approval (HAA), the well was drilled in 7/1987, is 140 feet deep, had a static water level at 4 feet, and is
cased to 33 feet(to bedrock). The well production was found to be 1.6 gpm on 2/10/1990 and the water sample results
for Nitrate and Total Coliform Bacteria were found to be satisfactory.
• There is a well located on T15N. R1W, Section 19, Lot 24 which serves a private residence. Based upon the 2005
Health Authority Approval (HAA), there is no well log for this well, but the well is 94+ feet deep, had a static water
3701 East Tudor Road. Suite 101 *Anchorage,Alaska 99507-1259
Phone:(907)337-6179*Fax: (907)338-3246*Website:www.garnessengineering.com
Page 4 of 4
level at 32 feet, and is cased to 40+ feet. The well production was found to be 1.1 gpm on 2/7/2005 and the water
sample results on 12/3/2004 for Nitrate was <0.1 mg/L and 0 colonies/100 mL for Total Coliform Bacteria.
• There is a well located on T15N, R1W, Section 19, Lot 23 and serves a private residence. Based upon the 2010 COSA,
the well is 111 feet deep, had a static water level at 27.8 feet, and is cased to 82 feet. The well production was found to
be 1.5 gpm on 5/8/2010 and the water sample results on 5/3/2010 for Nitrate was ND mg/L and 0 colonies/100 mL
for Total Coliform Bacteria.
• There is a well located on Thibault S/D, Lot 1, but no well log or information could be found for this well.
• There is a well located on Thibault, Lot 2 which serves a private residence. Based upon the 2013 COSA, the well is
102 feet deep. had a static water level at 36 feet, and is cased to 102 feet. The well production was found to be 5.2
gpm on 7/30/2013 and the water sample results on 8/22/2013 for Nitrate was ND mg/L and negative for Total Coliform
Bacteria.
• There is a well located on T15N, R1W, Section 18, Lot 205-A which serves a private residence. Based upon the
2012 COSA, the well is 75 feet deep. had a static water level at 8 feet, and is cased to 71 feet. The well
production was found to be >2.2 gpm on 9/10/2012 and the water sample results on 10/12/2012 for Nitrate was
ND mg/L and negative for Total Coliform Bacteria.
• There is a well located on T15N, R1W, Section 18, Lot 203 which serves a private residence. Based upon the 2009
COSA, the well is 200 feet deep, had a static water level at 41 feet, and is cased to 86 feet. The well production was
found to be 0.97 gpm on 8/11/2009 and the water sample results on 8/12/2009 for Nitrate was ND mg/L and 0
colonies/100 mL for Total Coliform Bacteria.
• There is a well located on T15N, R1W, Section 18, Lot 201, but no well log or information could be found for this well.
• There is an existing well located on property within this subdivision; however, no information could be found for the
well. On August 2, 2017, Wheaton Water Well, Inc. performed a partial video documentation (see attached Inspection
Report). On October 10, 2017, Wheaton Water Well, Inc. returned to the property and performed further documentation
on the well and also performed a 24 hour well test. Attached is a letter from them stating their findings. In short, the 24
hour well production was 0.99 gpm.
Based upon the aforementioned well records, it appears that water availability is reasonable for this subdivision and water
quality (in regards to nitrates and bacteria) is good. We are recommending a note be placed on the plat in regards to well
production. The following is the recommended note:
1. It should be anticipated that water wells within this subdivision may have low production. Water
storage systems may be required to develop an adequate water supply.
If needed,we can provide you with a copy of the supporting documentation referenced above.
CONCLUSION:
Based upon the test holes, records research for water availability, and the well/septic reserve site map, the proposed
subdivision appears to meets MOA subdivision standards and appears to be viable in regards to onsite water and
wastewater. If you have any questions, please contact us at 337-6179.
Sinc rely, .
1
Jeff•. r -r es P., ., M.S.
Presid- t
3701 East Tudor Road, Suite 101 *Anchorage,Alaska 99507-1259
Phone: (907)337-6179*Fax: (907)338-3246*Website:www.garnessengineering.com
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"PERCOLATION TEST PREFORMED IN ML LENSE.BASED UPON PERCOLATION RATE,
16 ADVANCED TREATMENT SYSTEM REQUIRED FOR THIS TEST HOLE.
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PERCOLATION RAIL '120 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19
TEST RUN BETWEEN 3 FT. AND 4 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: U YES ❑ NO
SOILS LOGGED BY: JODY MAUS PERCOLATION TEST PERFORMED BY: JODY MAUS
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG, Ltd. I,JEFFREY A.GARNESS, CERTIFY THAT THIS WAS PTRF
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4 5:12 30 3-1/4" 2-3/4"
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6 5:42 30 3-1/4" 2-3/4"
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PERCOLATION RATE 10.9 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19
TEST RUN BETWEEN 3 FT. AND 4 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: U YES ❑ NO
SOILS LOGGED BY: JODY MAUS PERCOLATION TEST PERFORMED BY: JODY MAUS
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG, Ltd. I, JEFFREY A. GARNESS, CERTIFY THAT THIS WA�RFf�RMED IN ACCORDANCE
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11 TIME (MINUTES) READING (INCHES)
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12/6/2016 1 4:00 - 6" -
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13 —
ABSORBED ONLY 1/4"- 1/2"DURING PRESOAK PERIOD.BENCH HAD TIGHT SILTY/CLAY
14 — SOILS. PERK HOLE WAS SCARIFIED PRIOR TO ADDING PERK SLEEVE AND GRAVEL.
15
16 —
17
18 —
PERCOLATION RATE >120 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19
TEST RUN BETWEEN 2.5 FT. AND 3.5 FT.
20 -- A FOUR HOUR PRESOAK WAS PERFORMED: El YES ❑ NO
SOILS LOGGED BY: JODY MAUS PERCOLATION TEST PERFORMED BY: ERIK WIDGER/J.L.M.
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG, Ltd. I,JEFFREY A. GARNESS, CERTIFY THAT THIS WAS P]RFO MED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: �/ 4�/7
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PERFORMED FOR: RYAN MATHIAS DATE: 12/6/2016 .•� P FESS\CP84�
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11 ' GM & ML DATE READING CLOCK NET TIME WATER LEVEL NET DROP
TIME (MINUTES) READING (INCHES)
12 • 12/6/2016 1 11:48 - 6" -
• 2 11:58 10 3-1/2" 2-1/2"
•
13 3 11:58 - 6" -
•
B.O.fI. 4 12:08 10 3-1/2" 2-1/2"
14 5 12:08 - 6" -
6 12:18 10 3-1/2" 2-1/2"
15 7 12:18 - 6" -
16 8 12:28 10 3-1/2" 2-1/2"
9 12:28 - 6" -
17 10 12:38 10 3-1/2" 2-1/2"
11 12:38 - 6"
18 12 12:48 10 3-1/2" 2-1/2"
19 PERCOLATION RATE 4 (MIN./INCH) PERC. HOLE DIA. 6 (INCHLS)
TEST RUN BETWEEN 4.5 FT. AND 5.5 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED:
E YES El NO
SOILS LOGGED BY: JODY MAUS PERCOLATION TEST PERFORMED BY: JODY MAUS
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG, Ltd. I,JEFFREY A. GARNESS, CERTIFY THAT THIS WAS PFO MED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: 1 - /4
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SOIL LOG - PERCOLATION TEST •c-% '' CE 795 '•r
LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION ♦ ! '•<(.
♦♦� •Fo° •••P� ••
PERFORMED FOR: RYAN MATHIAS DATE: 12/6/2016 �� ROFESS,I444
LICENSE .1►" m**
DEPTH — : ORGANICS #AECC884
(feet) - �. TEST HOLE #5
1
SOIL CLASSIFICATIONS SITE PLAN
2 —
-:y, Y G W ::::= ::: ORG
3 — s GP I I I ML
GM i � CL
4 — ji .:'I
o O
CH
5 —
1,11IM
Gj.k'• SM '� ,,/ OH �O
6 - e . SC
GM & ML e0
7 DEPTH TO
GROUNDWATER DATE �l�,Q'
8 DRY 12/6/2016
DRY 12/13/2016 SCALE:
'
9 11' 5/11/2017 1•=1o0'
10 —
11 DATE READING CLOCK NET TIME WATER LEVEL NET DROP
TIME (MINUTES) READING (INCHES)
12 12/7/2016 1 2:43 - 6" -
2 3:13 30 2-3/4" 3-1/4"
13 3 3:13 6" -
B.O.H. —
4 3:43 30 2-3/4" 3-1/4"
14 — 5 3:43 - 6" -
6 4:13 30 2-3/4" 3-1/4"
15
16
17 —
18
PERCOLATION RATE 9.2 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19
TEST RUN BETWEEN 3 FT. AND 4 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: U YES ❑ NO
SOILS LOGGED BY: JODY MAUS PERCOLATION TEST PERFORMED BY: ERIK WIDGER/J.L.M.
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG, Ltd. I,JEFFREY A.GARNESS,CERTIFY THAT THIS WAS PEORrED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: 4/ ( '
7
111 I
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. t•
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SOIL LOG - PERCOLATION TEST 0.�, ffr .79 3 ess':��
LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION •.♦�� .,• ., �:�
•
PERFORMED FOR: RYAN MATHIAS DATE: 12/6/2016 444
.e0• 2
•.-44 .t.(3.\,.
LICENSE �1li„`iik*
DEPTH ---- ORGANICS
#AECC884
(feet) �� TEST HOLE #6
1
SOIL CLASSIFICATIONS SITE PLAN
2
;::V. GW i:::::::::: ORG
` r+
3 GP j I I ML
4 GM8ML 4', GGCM �� < OL
Q°�°o 0, SW Jr)) MH �Q�
':•'••Ift SP CH �
5 GJ
r SM �� ,/M OH �O
6 vs
SC �`
P�'
)\
7 DEPTH TO
GROUNDWATER DACE ��P N
8 DRY 12/6/2016
j 8' 12/13/2016 SCALE:
9
CL 3' 5/11/2017 1'=100.
VISUALLYLY RATED
10 IMPERMEABLE
11 DATE READING CLOCK NET TIME WATER LEVEL NET DROP
TIME (MINUTES) READING (INCHES)
12 12/7/2016 1 2:40 6"
2 3:10 30 5-3/8" 5/8"
B.O.I1.
13 — 3 3:10 - 6" -
4 3:40 30 5-3/8" 5/8"
14 5 3:40 - 6" -
6 4:10 30 5-3/8" 5/8"
15
16
17
18 —
19 PERCOLATION RATE 48 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
TEST RUN BETWEEN 3 FT. AND 4 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: II. YES ❑ NO
SOILS LOGGED BY: JODY MAUS PERCOLATION TEST PERFORMED BY: ERIK WIDGER/J.L.M.
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG, Ltd. I,JEFFREY A. GARNESS, CERTIFY THAT THIS WAS PEfFORjvIED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: 9. lI
�\ ; * °,
GARNESS ENGINEERING GROUP, L •tdti-
9 ':..; •
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•
3701 E.TUDOR ROAD,SUITE 101•A'.CNORAGE.AK 99507•PHONE(907)337-6179•FAX(907)33&3246•WEBSITE:AvAvgrnasseegl"eal"9 com
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SOIL LOG - PERCOLATION TEST ��6 '•�' C 795 ;= ��
LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION �� ��`�'•.,• ����
PERFORMED FOR: RYAN MATHIAS DATE: 12/7/2016 ♦�1 P/�• ����� �1P����
LICENSE ,�IIivi„S``o��•
DEPTH #AECC884
(feet) ^ ORGANICS TEST HOLE #7
1 —' --
SOIL CLASSIFICATIONS SITE PLAN
2
''s '_::o:,• GW :,::= ORG
3 �
. �i_ GP ML
r GM CL
4 GC OL \P�
0 0 0 C SW 1 j MH �Q
o � ogo //}I
•••• % //
5 GM/SM/ML • •• •• •. SP CH �\
t SM ,' ,/ �i OH �O
rat SC
6 PG
ik
7 DEPTH TO
GROUNDWATER DATE <</4,P N
8 WEEP @ 10' 12/7/2016
6' 12/13/2016 SCALE.
I
9 6' 12/14/2016 1"=100
1.5' 5/11/2017
10
CL OR ML DATE READING CLOCK NET TIME WATER LEVEL NET DROP
11 VISUALLY RATED TIME (MINUTES) READING (INCHES)
IMPERMEABLE '
12/7/2016 1 2:35 - 6" -
12
/„ 2 3:05 30 5-1/8" 7/8"
B.O.H.
13 —
3 3:05 - 6" -
4 _ 3:35 30 5-1/8" 7/8"
14 — 5 3:35 - 6" -
6 4:05 30 5-1/8" 7/8"
15 —
16 —
17
18 —
PERCOLATION RATE 34.3 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19 —
TEST RUN BETWEEN_ 3.5 FT. AND 4.5 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: El YES ❑ NO
SOILS LOGGED BY: JODY MADS PERCOLATION TEST PERFORMED BY: ERIK WIDGER/J.L.M.
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH.
PERFORMED BY GEG,Ltd. I,JEFFREY A. GARNESS,CERTIFY THAT THIS WAS PE OR D IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: * ' 9 /g
J
GARNESS ENGINEERING GROUP, Ltd • *i� 49 �'* •
•
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3701 E.TUDOR ROAD.SUITE 101•ANCHORAGE.AK 99507•PHONE(907(337-0wwwm
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SOIL LOG - PERCOLATION TEST • 0 `• CE 795
LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION �•� •• -f''•
•PERFORMED FOR: RYAN MATHIAS DATE: 12/7/2016 •*et6'PROFESS\10\4 - .
DEPTH #LLECCSE84 ,,IIlisssik10•
(feet) ORGANICS TEST HOLE #8
1 —�
SOIL CLASSIFICATIONS SITE PLAN
2
d ?': GW :,=:::::::::: ORG
3 — .:': GP ML
e CL
4 — / 4GM
�IOLGM & ML 0°00°0° °c SW 11��� MH Q
••'•:
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3701 E.TUDOR ROAD.SUITE 101•ANCHORAGE.AN 99507•PHONE(907)337.8179.7A%(907)330-3248•WEBSITE'wxw.gamr<xngi rAn9.cnm . ..��• i• • • • .
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SOIL LOG - PERCOLATION TEST ���� 79 _�
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LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION �..�`N'•.,� 1 g.��:
PERFORMED FOR: RYAN MATHIAS DATE: 12/6/2016 •�,�IPRpFE ;�::.LICENSE �.
DEPTH CHRISTOPHER WOODS, #AECC884 I,������•
(feet) ��- ORGANICS
1
TEST HOLE #1 P.E.d
• •;•.• LOAM (SM) SITE PLAN
[''a SOIL CLASSIFICATIONS2GW - ORG
ML
GM J1 . CL
*SM 8 ML I OL
4 — WITH SOME Do°a os, 1
GRAVEL o°a°o° °a SW MH Q
•S• • •• SP CH -<<•�('
5 — r t • SM ,' .'1i OH �O
GEG 4... k.
6 — B.O.H. p Sc PG�
.,I—
DEPTH TO
7 — W GROUNDWATER DATE fie. N
—1— 5
8 — _ PER C.W. • - DRY 11/20/2007
~w PER GEG - - 10' 12/13/2016SCALE:
9 I ,
Z PER GEG - 6' 5/11/2017 1.=too'
D_
10 0 LL
O
0 Et
� DATE READING CLOCK NET TIME WATER LEVEL NET DROP
11 — wa TIME (MINUTES) READING (INCHES)
12 —
I
12/6/2016 1 4:10 - 6"
1-j 2 4:40 30 4-7/8" 1-1/8"
c/)0
13 — Q'Z 3 4:40 - 6" -
=
LU
CO 4 5:10 30 4-7/8" 1-1/8"
U
14 — LWLU
r 5 5:10 - 6" -
00
6 5:40 30 4-7/8" 1-1/8"
Lu
15 0
"CONFIRMATION PERCOLATION TEST ONLY. NOTE:SOIL IMPERMEABLE
16C.W. AT DEPTH OF 7 FEET PER CHRIS WOOD,P.E.TEST HOLE
B.O.H. •
17
18
PERCOLATION RATE '26.7 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19
TEST RUN BETWEEN 4.5 FT. AND 5.5 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: • YES ❑ NO
SOILS LOGGED BY: "JODY MAUS PERCOLATION TEST PERFORMED BY: JODY MAUS
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH. C.W.=CHRISTOPHER WOOD,P.E.
PERFORMED BY GEG, Ltd. I,JEFFREY A. GARNESS, CERTIFY THAT THIS WASF�FOF�MED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: f/i'f!/q
`
.�_.......,,i_
GARNESS ENGINEERING GROUP, Ltd 5
CIVIL&ENVIRONMENTAL ENGINEERS % • 1 0
3701 E.TUDOR ROAD.SUITE 101•ANCHORAGE.AK 99507•PHONE(907)337-8179•FAX(907)338.3248•WEBSITF�www ryvnesvm71Mv8Ing corn .
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SOIL LOG - PERCOLATION TEST ♦ 6-�:, '2
LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION •�• 77953
. jD.*PERFORMED FOR: RYAN MATHIAS DATE: 12/6/2016 � SS��•.•
DEPTH CHRISTOPHER WOODS,P.E. #AECC884 LICENSE 11����, '
(feet) ORGANICS
""--". TEST HOLE #2B
1 . .' . LOAM (SM)
�� •
SOIL CLASSIFICATIONS SITE PLAN
•2
a;�:o-'.'1 G W ORG
*SM & ML : ""r;-r..,.e
3 — WITH SOME ,(�jr)&
r`- GP ML
GRAVEL GM GC ./ / CL
OL
4
�T
GEG o0 000 o c S VV I)) MH Q
B.O.H. i.L•. ., SP / CH \4�
5— Gj
H aSC SM / ,,M OH �O
R91-12 `Z`
s 41 �PG
7— _ i,
Lu DEPTH TO DATE
LLi GROUNDWATER ��Q' N
8 — wO PER C.W. • SEEP @ 10' 11/20/2007
5
p0 Li_
PER GEG 9.5' 12/13/2016 SCALE:
9 a- PER GEG • -- 6.5' 5/11/2017 1"=100'
D_O
10 - W I-
=p
�= DATE READING CLOCK NET TIME WATER LEVEL NET DROP
11 — I-z TIME (MINUTES) READING (INCHES)
12 — =m 12/6/2016 1 4:05 - 6" -
Uw
UJ 2 4:35 30 5-1/8" 7/8"
13 — w 3 4:35 6"
U 4 5:05 30 5-1/8" 7/8"
14 5 5:05 - 6"
C.W. ,
B.O.H. 6 5:35 30 5-1/8" 7/8"
15
`CONFIRMATION PERCOLATION TEST ONLY. NOTE:CHRIS WOOD P.E. SOIL LOG SHOWED
16 I IMPERMEABLE SOILS ON HIS SOIL LOG BUT DOES NOT SHOW PERCOLATION DEPTH.
17 —
18 —
PERCOLATION RATE "34.3 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19 —
TEST RUN BETWEEN 3 FT. AND 4 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: • YES ❑ NO
SOILS LOGGED BY: *JODY MAUS PERCOLATION TEST PERFORMED BY: ERIK WIDGER/J.L.M.
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH. C.W.=CHRISTOPHER WOOD,P.E.
PERFORMED BY GEG, Ltd. I,JEFFREY A. GARNESS, CERTIFY THAT THIS WAS PERTOR ED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: q
' oissusILitmi
krl
tel\ •c I ��• I 4� , ♦♦
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CIVIL&ENVIRONMENTAL ENGINEERS •
3701 E.TUDOR ROM.SUITE 101•ANCHORAGE.AK 95507•PHONE(907)3378179•FAX(907)338-3248•WEBSITE:xwx.gamnz fir M9 cnm !• 'Y•••• •• : =
SOIL LOG - PERCOLATION TEST ♦♦�,��, ff R:Garrless
LEGAL DESCRIPTION: T15N,R1 W,SECTION 19,LOT 4-PROPOSED MATHIAS SUBDIVISION •♦♦.4,4...,, .
13."��:.
PERFORMED FOR: RYAN MATHIAS DATE: 12/6/2016 •/a'at.P FE S��Q...4
LICENSE 1 j"`����
DEPTH --; ORGANICS CHRISTOPHER WOODS,P.E. #AECC884
(feet) TEST HOLE #3
1 ;• •;i • LOAM (SM)
t
• •• •
2 SOIL CLASSIFICATIONS SITE PLAN
•
' : ,'.o' GW - : ORG
3 —; *SM ML .,,, GP
j ) ML
4—
WITH SOME 4j GM J//� CL
;• • GRAVEL GC 1 1 OL \,'
oo°�� c SW 1 oi MH Q
GEG .
5— B.O H. •• • • SP CH �
.
:!; t ' SM �i OHO
6— I- .. t., SC G��,
v;UJ P
7— =Y DEPTH TO DATE �P
1---c GROUNDWATER
w
8 — PER C.W. -SEEP @ 14' 11/20/2007
o CC PER GEG - - 9.5' 12/13/2016 SCALE:
Iii
9 — 01.1- PER GEG - 8.0' 5/11/2017 1"=too'
O D_
10 — D'O
w I—
i o DATE READING CLOCK NET TIME WATER LEVEL NET DROP
11 — Ow TIME (MINUTES) READING (INCHES)
C O 12/6/2016 1 4:04 - 6" -
12 — D'w
U m 2 4:34 30 5" 1"
13 — w LLIJ 3 4:34 - 6"
o c 4 5:04 30 5" 1"
14 UJ
O 5 5:04 6"
6 5:34 30 5" 1"
15
C.W.
B.O.11. `CONFIRMATION PERCOLATION TEST ONLY.NOTE:CHRIS WOOD P.E.TEST
16 — I I I I 1
HOLE#3 SHOWS IMPERMEABLE SOILS BETWEEN 4 FEET AND 5 FEET.
17 —
18
PERCOLATION RATE '30 (MIN./INCH) PERC. HOLE DIA. 6 (INCHES)
19 — -
TEST RUN BETWEEN 3.5 FT. AND 4.5 FT.
20 A FOUR HOUR PRESOAK WAS PERFORMED: • YES ❑ NO
SOILS LOGGED BY: 5JODY MAUS PERCOLATION TEST PERFORMED BY: ERIK WIDGER/J.L.M.
COMMENTS: PERCOLATION READINGS ARE WITHIN 1/16 OF INCH. C.W.=CHRISTOPHER WOOD,P.E.
PERFORMED BY GEG, Ltd. I, JEFFREY A. GARNESS, CERTIFY THAT THIS WAS PEORI4ED IN ACCORDANCE
WITH ALL STATE AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE: 7
9 / '
f.
A1 !! !� M�\%!t'! T.�ATf'�TATF:etIrl6v-wr.-•. m'�c o' A/ �N►.
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A. 10421 WW RD, SUITE 201 F GJ` I<t
37
EAGLE RIVER, AK. 99577T1~ �J�al .tet'.
(907) 694-5195 FAX (907) 694-7')(17 /• • . .'. .%`,..- -/.%i% • /7 f
SOILS LOG — 0• • 6.• '. .. ..L:
PERCOLATION TEST 1, /h'.c�tRISCE,o E7. ..... 0
'4',.":0 �� X
4.1
PERFORMED FOR: RYAN MATHIAS
DATE PERFORMED {I _ <',._%:?.
' Ikka orESSI0t1�\ +1�'
LEGAL DESCRIPTION: T'SN, RIW SEC. 19 LOT ^
TEST HOLE # - — TOWNSHIP RANGE SECTION T 15N R1 W SEC. 19
DEPiH SITE PLAN(Nf)T TO Cf At rl
krct.1
I I— -.
a
i I
--l.%' / vs" I.r it , a.,,
1 5" ATTACHED nn nED SKETCH I
._JI ,r. 1L. _ t
H
r n
SIS_-- - III
is_ ,..,, ,. I !!,
91 4 S1f ALC ?' r ,� f
'I In'!:'I `' - i -fV1.1-7A--1—ER 1"A nnre—,
El
TERLEl I ^
14 i 15 '�I 4•
16
PERC TEST RESULTS
Rcr+uiNt.i DATE GROSS TIME NET TIME DEPTH
1'--I TO WATER NET DROP
u�7; r «: i.----:.ma _
18--I • �:4;'�
11
1111111111111111111111111111111111....1
1111111111.1
2.
z p—I I------I I.
22
RERCOLA-now RATE= i f, , (mewiNCH! FERC HOLE DIANE-S2=6"
TEST RUN BETIAEN ..7 FT ANr1 ¢i 4-7-
____
• 'WhzENTS• `—�
S01L ,0•G,Ggg EIXj CHRISTIIPHrp omen
,,. — — -
•i:: ;� PiRCOLATION TEST BY: CHRISTOPHE r
11����1`�''�/%�rn� s�i'. CERTIFY R Y;00;;
THAT THIS TEST WAS PERFORMED IN ACCORDANCE WITH ALL STATE
AND MUNICIPAL GUIDELINES IN EFFECT ON TI-tig DATE DATE: 1n , 1 /
EAGLE RIVER ENGINEERING .a�P's ' • • • �,,.��
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(907) 694-5195 FAX: (907) 694-3297 s' '
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SOILS LOG - PERCOLATION TEST .`"RISME;o R. W000.4
PERFORMED FOR: RYAN MATHIAS _DATE PERFORMED �I/� ��p ��� \r E5s1oN r ♦+
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LEGAL DESCRIPTION: T15N, R1 W, SEC. 19 LOT 4
TOWNSHIP RANGE SECTION T15N. Rt W, SEC. 19
TEST HOLE #
DEPTHSITE PLAN(NOT TO SCALE)
(FEET)
0
VVVVV 1 f BRq wN
2
-10eca L-
3
S /M SEE ATTACHED SKETCH
4IMO vJ IJ
5 rt S1'rLK`�
6
s •
a L SNAL6 001)510
P Tr
inDATE
WATER TABLE DATA
11 WATER LEVEL
12 �. •
VERY"ac,tir
13
14
15
PERC TEST RESULTS
16 READING DATE GROSS TIME NET TIME DEPTH TO WATER NET DROP
17
18
19
20
21
22
FBRCOLATION RA i(MWNVChI) FERC HOLE DIAMETER "
MST F A D FT
:OMMENTSL ""r" :(>
SOILS
I�.Q✓ CHRISTOPHER WOOD PERCOLATION TEST BY:_ CHRISTOPHER WOOD
I c.7---/
!//�" " CERTIFY THAT
THIS TEST WAS PERFORMED IN ACCORDANCE WITH ALL STATE
AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE. DATE: e71l20/j
..
AEAGLE RIVER ENGINEERING `-PSE of 1..0
10421 VFW RD, SUITE " 1
EAGLE RIVER, AK. 995771 s,k H N):;•70 •
(907) 694-5195 FAX: (907) 694-3297 ,j * //
f �� r
r
SOILS LOG -- PERCOLATION TEST '#`9 ..CHRISTOPHER
CHRtS 10 87"0°.
,,, "
PERFORMED FOR: RYAN MATHIAS DATE PERFORMED II/2c)/o t1,�ZM ESS10N���♦�
LEGAL DESCRIPTION: T15N, R1W, SEC. 19 LOT 4
TOWNSHIP RANGE SECTION T15N, R1W, SEC. 19
TEST HOLE # Sr
SITE PLAN(NOT TO SCALE)
DErt}1 _
(FEET)
0
1 SILTY l'PSo%L
1,
2 V/ VO
3 e J' J
/%'' TAN SMkML SEE ATTACHED SKETCH
4 r -
,•
5_, 1T .
f /;
6 Si
T' ML /SM
8 r •', wtsMALe• •
9 /A ,
10 WATER TABLE DATA
DATE WATER LEVEL
11iii
12 C13414
14 Si
15 4
PERC TEST RESULTS
16 READING DATE GROSS TIME NET TIME DEPTH TO WATER NET DROP
,� I 11(7/4.27 //: 0 y L $ ' //6
Z / 17.:v( 3o y'-, 344 '/4
18 3
12.:01, Q 114-'3 IYZi•
19 I _3 L
20 S 12:0 0 `t•-e6 's/L
G 1 : o7 10 4`--9 744 3//4
21
22
PERCOLATION RATE*."(VIN/IFERC HOLE Dt41uE = '
.LAST RUN BETWEEN / F•T_AND c FT
:OMMENTS• 5.1
vaaryr cep•' ,
SOIL y") E1 CHRIST PHER WOOD
�� �IS° PERCOLATION TEST BY: CHRISTOPHER WOOD
CERTIFY THAT THIS TEST WAS PERFORMED IN ACCORDANCE WITH ALL STATE
A D MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE. DATE: 9/20/045
4,...‘.,:r.„:4*4.1!.••••,•;..,qt..
„,, < OFAi k
44.
EAGLE RIVER ENG-"17`-,TERP Mr!
',.‹. - V.:1,1:4'
1-1—k--
, ik 104.21 ww an cl./Iry 2r.”
LAGLE RIVER, AK. 99577 :71/47J/200.141 "
(907) 694-5195 FAX: (907) 694-3297 e 1 .",./417/".e.e., , 1 •.1' •••
1.o.10.1%4'e i,r V
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SOILS LOG - PERCOLATION TESTr•--., .04FlisTorHER R. WOOD: Z'AII
f'CI • *
41 .5... . C1-io3B7 • 47.!"
'C.42) • • • . •-,..-Ai
4,
if
'4 lk PlitrE 13' -*e.
ilk• 55191A ..,'•••
PETZFORME.ii FOk: IAN,1,4A'MIAS DATE PERFORMED ik 170 I r,:i.
14.,tota,ixs
....._ __________
1 FnA.I 01:-CrClicu -el e . "..... ...-- .
• • ..._,..•...„.,,,...2:,.i.-..f.,_,:,,_,C!...,...t..1 LV I 4 . _ TO94PANC.:..c: S.FCTIC:;...7:FN R;:7 3EC. la
If:SI HOLE # 4 :,!
LIK Pi./IN /4M -I _
(FEET)
1
_
i
I 1
1-40Ji4P A isi'llY 7oP54)7 1...
I
I
I
- fr_-,.....,+______....____.._..
- i 1 1 -!I 1
—11 ci l' • % '.
•
ii -• ' .
---11 i i 1 I 5.11 i' fA,..1!)-i
t I 7 r
H I
- 7-11 t II
/
i
i
----------:::-----------------‘.'"N 1
DI .1 I I WA-TER -A r 1------------------ ----)
.„ : q •1 ! DATF-1'-17n7,T7R,---.7i-E77F--i
. 1 -1 4 1 1 t___________I_____________„.1
1130 1 -11
1 ----.
/2 i /- i
l! / 1 I
i..s i.„ , .11
1411 ill
!
b., :- 11 %Nit
..
PERC TEST RESULTS
18 _____
READm wF----lj--7---E GRosR ,r---Tuf.a.rwr .4.' CCM-II TO WA'jar( I. ORt3P I
i
7—f a M.:-/ 41 P. C.?
1.
-------.-- , - •' "- - 1/.•-'• .. •t.,
:
I // fin a• I :0 I ME= . .0 • 4 "1: 4.::
184 1 /.,„ E.,,,c,ccx. ,i-..
2 • ,••••• 1 1
. ' 1
I
:i - 4 '..'• I •
LtI---1
1 ;
•
i_ iL__. __ _ ___J_
_•_.•.. ,_:::•.,,:. • 7 i/ ki•iliViv:..;rii FeRCI131.ErlArrEng4=T
( LIINIBEKL_I.iFT Am? I. FT
rwatico.rrc--
_ .. .... _.. _ .... . __ ._
• --•----------—• --- .------- - - --- — -
JviL. LOGGED 14,0 (1-11;11.,rOPHEWO0()._ ___
PrqCOL.4710:4 1F-cT R'.' rt.tolr•••••••%,,..-,-. ...-. -
,..: •1 ' e.14 ''-''''-e...rIrPTiv 1-4.'''3. 7 '. 7L-51 ri.•:%:-.. ;',/..!-,:t:ORMED H.! A(,.'.1-4-1nD6..NcE %.,. ALL s TA TE
AND 4;UNICIFAkt_ uult)ELINES IN EFFECT ON THIS DATC. CAW: ' ?//:•),/,........,„•::
AEAGLE RIVER ENGINEERING ...„ OF. „V ‘44
10421 VFW RD SUITE 201 ;;c.) . ,(.- fj
EAGLE RIVER, AK. 99577 0 * r9iTH /., r #
(907) 694-5195 FAX: (907) 694-3297 ' ' • ;
SOILS LOG - P + %CHRISTow1ER R. .'• f
ERCOLATION TEST T J, •. CE-10387 ' �Wt
PERFORMED FOR: RYAN MATHIAS DATE PERFORMED 12/d 3/ �+,4%y SSION PL�44IP
LEGAL DESCRIPTION: T15N. R1W, SEC. 19 LOT 4
TOWNSHIP RANGE SECTION TI5N, R1W SEC. 19
TEST HOLE # 4,-8
OEP7H — SITE PLAN(NOT TO SCALE)
(FEET)
0
13 2vw4k)
ToNc
2 ••
L
3 13�ow6oJ
`j Ni S (A) SEE ATTACHED SKETCH
4
5
6 - . Sw GO
7 J_t>
e -, 00.
y .
a -
10 0 WATER TABLE DATA
DATE WATER LEVEL
11 C-
12 U 6
13 Y
14
15
FERC TEST RESULTS
Its
READING DATE GROSS TIME NET TIME DEPTH TO WATER NET DROP
17
18 rr M i�� N -
20 IIIIIIIIIIII
-_-_��
22
21 -__
S L 1 -
LAT)N RAT (^' H) FERC HOLEDAIMIER-s•
TEST RUN 131..MN_t-ELAN r
)MMENTS
SOILS < CI IVlIST ER WOAD
PERCOLATION TEST BY:___CHRISTOPHER WOOD
CERTIFY THAT THIS TEST WAS PERFORMED IN ACCORDANCE WITH ALL STATE
AND MUNICIPAL GUIDELINES IN EFFECT ON THIS DATE. DATE: L/(2c)/0 ci
EAGLE RIVER ENGINEERING =;\ 9•F: s'#.
10421 VFW RD, SUITE 201 Com)•• i ��.- • �+
EAGLE RIVER. AK. 99577 i * �.1 .. +0,
(907) 694-5195 FAX: (907) 694-3297 ' ' ' ' ' '
SOILS LOG - PERCOLATION TEST `+,`s *CHRISTOPHER R. W000..,
c.�
PERFORMED FOR: RYAN MATHIAS DATE PERFORMED Zf(?�?/(�-1_ *r ssIoN ♦+'
LEGAL DESCRIPTION: T15NR1 W, SEC. 19 LOT 4
TOWNSHIP RANGE SECTION 115N, R1 W, SEC. 19
TEST HOLE # 4-p SITE PLAN(NOT TO SCALE)
DEPTH
(FEET)
0
���� 13R04.nrN
1DPsv?`
2 S M w/�,h.AUiL
3
SEE ATTACHED SKETCH
4
5 - 4
6 -�''' S�} W/ ,WaL
SMALL Stela
vQ
a "v
a- 0
10 0 ,
WATER TABLE DATA
11 ,0 u DATE WATER LEVEL
12 V =-
13
14 M Q L'A G L ==
15
'ERC TEST RESULTS
16 READIN11 GROSS TIME NET TIME DEPTH TO WATER NET DROP
17
A RiZETNIIIMElriPM11111
16
19
20
21
22.
I:IMOlA-DON RATE=< / (MIWNCFO PERC HOLE DIAL ETH-g�
_T_E.5RT UN BETYVEFnt S FT ANND k, FT
;OMMENTS:
SOIL •GGE• CHf�IST PHER WQQD PERCOLATION TEST BY: CHRISTOPHER WOOD
I � '
���� �-r-ICER71FY
THAT THIS TEST WAS PERFORMED IN ACCORDANCE WITH ALL STATE
AND MUNICIPAL GUIDEUNES IN EFFECT ON THIS DATE. DATE: of ,/0�j
IJ:•ct vTW RU, SUITE 201 ^ -
7. _ -'C.
".:L_ ,.....CT. :..x577 ..
(9:-)7) da .rig F.A.. (907) 604-1297 .�,
S('1LS LOG - P RC/LAT! '; ,. Tt-. __ i `. • _. .
PFqFOR1.1FD ;-np. n iri�i Tf'l1/tlJ 'e'i `.4
. ,Ah - ._ -- —DATE PERFORMEC i! t "77
•tom q ��ems` ►
LEGAL 4ESCRIPT!ON: 1.15N Ply/ ccr +r. g....7.7- —— ...... TOWNSHIP RANGE SECTION 1154. R1W. SEC. 1g
c- I
DEPTH
(FEET)
__ _ 5 li: saL�NtN(3T TO SOALI�
1
1 1 1
I
if.a r —
°-1 is .'s,;' r
0 ... I;r....;Ii....‘ill a
: :.
i i _..
1
. ..; ,::..1 -,:—It.•,' '1..u.,r , ./-1.," i
r
!
I
f
H:! f 1
40— I 1_ .ii:.C.. ,SELL-0/41A 1 _._.. __ --- ......_... t
1s--1 I
! I
��- FERC TEST RFc a Tc
i ` In_L=iiifiiVu DATE 1GF O. 'i1i ETaiEl x�."."r_
•
1 ,r^Tl l ^�.Ell: "� _
_ .. Ia -t 1 -- !I
1 I i--r—�--. i-'--_. - i___ __ a - i--- . �— -• — . _ Ii I ;_�� I_... !
1 -I- •I-- i { ! ,
I 1--_-_I._ 1 ._ 1 -I .— • _. .-1
1 — --- _
PERGOLA TON RATE= rArmytron.A — I _ __i
r'W.-A C.v.n.r.+r
a4iLytF4ki — I A N'1 ._
'n1.{f.fEA1TC•
SOI. 1,47.,13:..::. ; .4
• .r CHrif QPHF-RJ/Qn0 _
L
/4' ES. CI•IRISTr?ruF.R wenn
THAT THIS 1T:ST WAY P!r-n' r En
bNl. uirnlfrlAA` �.`.I„r.. - � , +�••,-,� i.•i .•',C;t;(}FsUAtdC;t WITH .411 �:I'a7C
Eur•IE3 IN LI-Hier ON THIS DR 1E, 11Tr ' ___ _,ice .
•
,
,41 , J If:
V.4'
_18
• fla
EAGLE: -IT"'‘1I4IR ENGIN-PI:P.PING- „...-r..s:" . • " • : -••'Y ri'4",
.. .• .,
71.4
A..: .A. V .F.-.1
• ...1.•..,1 .1.
F':r.,;' • •• i.: -. .1- 4•-
•.:•z,.:-:;-
i cik “..14.2 1 "Ft. RD. UI1T 201
:4-a..- iii"....J.i" I ;.;;•..1- : --. 1
r../1:..a.L Colit.i;. Ak. 977
•, " .y .1"/:17.. /
(.407) f.:94-51.95 FAY: (907) 69,1--3297
-,. - .. -. -•-• •i. ' ‘--. ' i
SOILS LOG — pF (-)
i-,-i-. —1 LIT'ON
. • _ — . • • I 1 . TEST .. 1 CizE,r- T)
357 Fr
•-..F"=
..,.. ..„
'4/0.;.'-' ..r•
•••
^.1:11FMNIED FOR: .. 1 :.:Ail i 1 ,:ilAS DA IF_ rEnrc,RvED_,, : ,H.?- '''4v., '...i'...-,-,.,,,.,t,o, ..,-4-.•
‘IAA:T,--;..-c.''4,-.•
-----
I EGAL OrSCIZIPTIAN. rl cht c.,44, e•-••-. • ...-
-. . _ ._..,..7,_!....e ..........,_... ...1_ . _ I OWN SHI P RANGE SECTION...MN, R1 V,/ SF-c. n
TEST kOLL #4111_
SI TE PI AIJ(NOT To c•--$1.
DEPTH ..-.
rs
(FEET)
• - —•
;
1
i 1
:
i
I I
13 87.e-)...)....,) 17...pc,,..;:e.".r)
' I
I
I
1-• I t A3 uqt.0A t)I-) i
.... 1 •
--- ..-•, ••-•••:.:-.,-; .,,,r.i tai
I .
I
4.i . • i -.• .
:
I
• 1 4 T-A1,-,' cl L A Vi• y
I
1 I.:
1
I
i I
f- 4 I !
I
I
I
• .
. — ,.... i
i
__ _—...f.:. I
——_-___ _..._ _ !
i ‘A"....•‘1-77.-P.T—"*..T.11:E. DATi-7-1
• , t
_
..!
- • A L....U.*. .4"/4:::i!!1,:iv.... -......'''..."''."'.7. .-.---..... -... .-'-'.4
•
. - -. ..--.•., ,
. _______. _.• _____
•
I
RE*C TEST RESULTS
/ I
17--1
I I mcm 1-111%!(..: !DATE IGADEtiiiiitiF7=1-itur inPD TY 7577-•,: .;.:." TIT:*Z- ...' .
____ ..... .
Kti.11.1
"H 1 L ._...... I P h-i- t.'i(' 7r ,
1 i
1 1 i
—
i I i i 1 —
-F. --— — • -----
-—...__t_____________I______-_
_ ... • —..I _ ._ I_____________I _._._____I
i&—1
1 - - I
---------la-----;--------— ..--._ II .__ ..
i
I_ 1
---"T" '— -----------'.. -- .----!
I ____,......_ I. 1 . .. 1
.. . 1 — ____ _________i____ —I
.i ------ -I--. __ ________ _ ....
_ _____.
PFRCOI.ATTIM PATF-: mv.,...!.. J..
7.7._. _j fts..414_WETW_E.EN . FT AND 71-
Outart.:Tt. ..
— — . . - .. . , AlliiIIIL.._,4- 77 .
_ :,-,41-1--:: : : . -. ----. --- — • • —
— ...— . • -....— ..— -- . __
SOIL 1...tiGGE.1) al: ul' J.-)Pli En WOOD__ _
PERCOI A TION TEST
s /////? / .,
i .. WA 3 PEI-6:0:04. ED IN ACCORO ANPF ‘11!TI-I ALL STA TE
• "LCFRTIFy "'HA 1-
A LIUNICiT;AL G WO h1.1141::S IN P•FrErl- ON 114r.. DATE. DATE.
�"...!'-`,.'t
� NN 1�' { ( u.
� LI.J M. Y L EN G + ry1 r.— ty ^tl c
EE ,•iY "ii
^i;�2i i'I W ItL) SUITE 20114.
Ar r_.-,' . --71!"-, . tF.
EAGLE RIVER, AK. 9950
J `.
(907 4--5195 FAX: (907) Fi94-3297 t. .". ( r •..,, %. . i. ...s
SOILS LOG — , . .
PERCOLATION ~
TEST s zsmriz:: Fi *OM ;y
CL-10367 °'r
+4 �',�
PERFORATED FOR: RYAN MATHIAS •
+ v;
-- . .._
DATE PERFORMED II/20/0?Z. �4-X>A,.t�...**--tea
LEGAL DFSCRIP/1OP!: T!5ts1,21.,V, !K.^ 19 ::,- .
TOWNSHIP RANGE SECTION T15N, R1W SEC. 19
TEST HOLE # 7 -,
DEPTH - — SHE PLAN(NOT TO SCALE)
o-
2 --
3
i SFF ATTACHED =X:1Y1:
CAA.,h 1 r
`t 1.1
j1''1
:ij
a.
./...- Com' b/+r►'h•Q
9 / C L WATER TABLE DATA
DATE WATER LEVEL
lo
n /.//
,z Kyo 142.0
. 1N.-., -,:,---..."
1
14-
15- {
PERC TEST RESULTS ti
16 READING DATE GROSSTIME
��..�� DEPTH TO WATER NET DROP+7
Z Wag
72 30 Pm 0 - 6 MM.16 :00 SO -s- $ . t
3 " S.L$�r� 3+.b �
19 aillili LI
20
mriiiire.imi
.....
z1 MEM=
zz IIIIMMUMINIMIIMUM1111
PERCOLATION RATE tris s. • PERC BOLE DWMETER
R V.a 6 _Pfls!aY,FT Anln Ll FT
:OMMENTS`
1
SX-9,27
- 2 9 Y: CNRISTOP�{ER WOOD
/j� PERCOLATION TEST BY: CHRISTOPHER W000
CERTIFY THAT THIS TEST WAS PERFORMED IN ACCORDANCE MTH ALL STATE
AND MUNICIPAL GUIDEUNES IN EFFECT ON THIS DATE. DATE: Z_
.• 401:I.ERS'SEAt s
•
'•
o :4 _ . .1*i
�� Munlctpattty of Anchorage • le4�••���e•44�44�44
DEPARTMENT OF HEALTH&HUMAN SERVICES • ��i1;1Ne`"r.:. / • . ..:
825`L"Street, Anchorage,Alaska 99502-0650 I�% DovW R. Dayton t 4;'
SOILS LOG�— PERCOLATION-FEST �9�s��•••4 Hao• 2205-E:,.
. 7 9;•- . i
PERFORMED FOR: ,13C.4 ,49 /Y4 J?2, -eT 71-- DATE PERFORMED: IN.kl.
LEGAL DESCRIPTION: T 4 r 5^' Township, Range,Section:S,/g Tj,,S-jLl X.,/it.)
DEPTH SLOPE SITE PLAN
(FEET/ Q$d/C- I 4244/1iJ/G$
N
• 2 ,,.f
3 - '? '1
4 - .
•
g.
5/4-Tri 40AYEG ..
7 - - .
8 ..
•
9 - .
10- WAS GROUND WATER _ ..
ENCOUNTERED? Yes
//° t Y S ,
•
'�sf/0,jlr IF YES,AT WHAT - i :_ .Q
12- • DEPTH ?1 P _ ,
E
/33 Depth MIN Alter
� b •Wa . ..
W 1K t�L Monitoring? fl0 Dila S// 9Z -
14- �6P Gross Net Depth to Not
Reading Date Time Time Water Drop .
15- •
•
16-
17
arrc++".CP 1-1t.eer - -
18-
19-
20-
PERCOLATION RATE (minutesiinch)PERC HOLE DIAMETER
• TEST RUN BETWEEN FT AND FT `
COMMENTS - •LG'ti 004s-7u/et " 6/0,"4,c /4/ /d"/3,/Lch� 4o 5•E. 0/ %/r1. Z
nn s‘,.,ya•n Fie v
/0 _
PERFORMED BY: .1).F— . 1 , •� , - CERTIFY THAT THIS TEST WAS PERFORMED IN
A.'.
IUr1UHt w NL. I t HALL b IA It ANL)MUNIUI NAL UU1UtL1NtS IN thW
l- I UN !HIS VA IE. VAI t: ��l/C/.• —
72-008(Rev.0851 '
• ir4 INEER'SSEAL)..+ v%�
• .._.. .. ..._. . - . . . .•. .y lig
•
"ter ;'•,, tr„ IS-7 l L
•-T.( J:• -4 14 *
td, Municipality of Anchorage 0 i. v
or DEPARTMENT OF HEALTH E.HUMAN SERVICES , e,—.....•.....4"
' 625'L'Street,Anchorage.Alaska 99502-0650 y ; David R. Dayton 1•t
s % NO.2205•E ••.Z.'
SOILS LOG — PERCOLATION-TEST e ,��,•• `
sr . . • 4 d,40FL510",�'
PERFORMED FOR: £C/M/i /f
0 A �iz/„7_ -37r..„-37r..„r ' DATE PERFORMED: Z
LEGAL DESCRIPTION:6;5✓T /or". ¢ Township,Range.Suction: /9j 77.57V, 2/iv
L9 — DEPTH SLOPE SITE PLAN
(FEET) --TCP Sult.. jt C9.04ita.VC.s 1
1 _
• N
3 --
aV'>r,- 6./7er eiZF
6 -
7 ` Si LT`� CKhtllist.
8 —
9. . :: ..
- . - 10- ... . . WAS GROUND WATER;', ii,2.e .. ... •
• . ..
ENCOUNTERED? /
11 - ....._.• : •._ _..:_._;_ S . . . . .. . .
IF YES,AT WHAT • /5` ' • . .• .
• ..O
. . 12- DEPTH? P
E
Depth to Watu After' ,•/'o "" '•,,.: -' -
13 1 - Monitoring? . '17~"" Nit e - - —
./e _ L _'
/ - 14 ��O'�� Reading Date Gross Nit Depth to Net
'
Time Time Water Drop
IT L . 15. 'it. t„rA-tZ»'L 5."c302 S7/o L /Z 'Z O 7+
iv/L. 30 0 42i. . .
16- /3-'/)1 . O 9 3'�
. /3.141 34) e 'Vet. 4 _
•
. 1T- • ,
18- / Y o 6
•
19- •
201
PERCOLATION RATE (mirwtcs/ineh)PERC ItOLE DIAMETER .4'
TEST RUN BETWEEN FT AND FT
COMMENTS' //raj. Sr ,,L(,rr '7/2cSDi9,'a-1J 01/C%0.f//l/fir /947/d/L J ) /1757"'
•
PERFORMED BY: l✓•re -aA) ir
I / ' A ...Ea. CERTIFY THAT THIS TEST WAS PERFORMED IN
AOOO(OA 40C WITI I ALL ATATC AtID MUI•IOIrAL OUIC LII EJ IIV Errec,T veil Tr•W VATC. DATC. e���.4._
72-008(Rev.U85)
C I I I' 1 I 198A I 197B I 197A I I 2 I /,/ / // B c0
WI L--
--H- H- i_ I / O / 0
H .W1 1-
1 1 yi I N 1/2 OF LOT 202 1 6I / O / i I ce
�1\Q�iO I I <I I I I 1 Q� 2 / �7 205-C i I N O w
0‘.4 ��p\ I I g I I '� I I.0 00 /\ I �, it
.� o / I I — w
I I c I dir)
---- --- 203 $ x_:25 —� / / / I -----If-----4t--- m trI I NI I I I � � g�, / G� / •, U
I I I I I S 1/2 OF LOT 202 1 I / /� / ' �� I w 0, p
_�{ PROPOSED PROPOSED SEPTIC LI / 1 / �\ 205-A I / I I 0_ W
I I I 201 I �►CJ, 1 8 BEDROOM SYSTEM SEE SEPTIC I m `/ // / I u 205-8 1 I 0 -1 CO
p
Section Comer La • 4 I I DUPLEX PERMIT REQUEST I , / w U 0 Z
i erPon.. I 1 ' I I I -•= —/ / L � _L •--J-- 1 ----/ \r --- °i 0 Q
Seo 24 1 / �� cTWIT"
ISPRUCE CRESTZI—. ��d��`���, �.. • ', L C.W. — I �SE�. , � � z0� Z'7 / TM�r 1 Q CO a w
it,
tiwt �,/ :: "'!, <, ; � / I Ii� P. xg
/,' \ ..4‘ ,Ik.---41P/se,4,4t.,. . ...
J ;`� �� '��►� of I 1 0..-1 W o o w
100i NW
/ 40
I o .
STREAM SETBACK / I / Ill �` _ 1 25**- -74k4fA/
4 -r �--
1 22 I-
---1 '(- ''7ti 1 '% / 18.000•rsa.FT.
N W
N / i ��- ,4: /// 18000+-.-FT-. ' SEPTIC RESERVE AREA ( w - x
\ �EPTIC AVE AREA ,/ 100'STREA SETBACK 1 I = O Q r
/ W
SCALE: // 4/ i� / �� IS, t...6_# / \ I 0 . -, 01
/ c.w.TH•4D y ` oay to 'q �� / \ \ 25 26 27C 27B o z g c N
1"=100'
c.w.TIA4= `\ /�SQ•JQ��O /O /� \ SERVED BY ww i w
// , Offillhl
'm 1 „ `a 0E pc o�` �/� . 0� \ I � PRIVATE WELL I a f a o 0
/ / ` 1 t t* 1.. / 'CZ
// 1 1 AND SEPTIC
// SEPTIC RESERVEAREA / 111,01k .1. �` 4 / 1:� , OO // 3 I I
/ // / p � I / Df 4 2 ey - ++- / /OOv • //v GRACE BRETFEN I 'I I
I S
// // / .„ + y `RILkeStrtJ/GEG TMs4 4fr' 5 'i1A
'iik.-.:. '''.' (..�2• Q- ./ -� i"_ I��- ,/ c.w.THr4c . f / �, �� M. It'/" - �., w. _ I� / 111* 1U II A' �;a ;: r --'" I C
IA
I .."::;-.21:1: c. 0-4i
IP% / ,5=6, ,,,.._ .....,. ,„
/ �� , �1 / / % 17.!..!-3,;::,.!..11:71
I W I / Z W
- / -1 49 GEG THOM ��� �` ', �r/ / \\ I II .
/- / nO\v\ C.W.TH/2A •� eiNi���/�j✓ S / \ ::•••".!%,
I I U)1 C I 1,-;
`G�V // 78.000+SO.Ff. \ - �' W 1W1 Wv
/ ..J GEG THC2 ��,���/ / SEPTIC RESERVE AREA N. 9` "/ C `4 Q I r + • W Z�
/ / r . e` / I os
'��• �/ 100'STREAM SETBACK VC:y6,`A l id =1 I ,
ALL GEG AND CHRIS WOOD,P.E.TEST, id `• c.w.nun / 1 / FO ep`4`5� I I �M w
HOLES WERE PHYSICALLY LOCATED IN , // `\ � � / DD I -—� g �p�———-� 44 45 4-1'
THE FIELD BY GEG AND THE LOCATIONS ' .w.TH/2 \\ / 5 I I —
MAPPED BY A PROFESSIONAL LAND r
SURVEYOR(S4 GROUP,LLC) // TRACT �\ � �
I (if ,::- I
Gw'""" 416 / 14.000+SOFT � � \ / I L K AND R STREET J W
GEG TH•1 SEPTIC RESERVE AREA 1 / - - - - - -—-—-—- — — —
/ , /
DRAWING NOTES: / T1�
• PER S4 GROUP, LTD.,THE SLOPE CONTOURS / / �C.c
SHOWN ARE 2 FOOT INTERVALS. I / / / O�Q �Q\J ( �. •,�•,•.�.�•
• GEG=GARNESS ENGINEERING GROUP,LTD. I / / OJ\ �cv �'��$N-.."""'"•" ••���
• D.D.=DAVID DAYTON,p• C.W.=CHRISTOPHER E. P.E. I / / NS�� �m 9r.i
• D.D.TEST HOLES AND GEG(2002)TEST HOLE I/ / J %• �SEE22 N.M1:: •
i FOR$.GYEJ OR •.il. j
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Preliminary Jurisdictional Determination Form
Nov n
This preliminary JD find that there"may be"waters of the United States on the subject project site that could e affected by th41l&oposed
activity based on the following information:
G �o
District Office Alaska District Office File/ORM# POA-2015-545 PJD Date Oct ,
State AK City/County Chuglak
Name and
Nearest Waterbody Fire Creek Address of Ryan Mathias
Project Person Post Office Box 110818
Location Section(s) 19 Township 15 S Requesting Anchorage,AK 99511
PJD
Meridian Seward Range 1 W
USGS Quad Map AK-Anchorage B-7 Latitude 61.3815 N Longitude 149.5374 W
Subdivision Name,Block,Lot,
Directions to Project Site Municipality of Anchorage
Identify(Estimate)Amount of Waters In the Review Area Stream Flow Name of Any
Non-Wetland Waters; Water Bodies on Tidal:
the Site Identified
1,255 Linear ft Width L Acres Ephemeral as Section 10 Non-Tidal:
Waters:
Wetlands Office(Desk)Determination
Date of
2.569 Acres Cowardin Class: Palustrine,emergent ❑ Field Determination Site Visit:
SUPPORTING DATA:Data Review for Preliminary JD(check all that apply-checked items should be included in case file and,where
checked and requested,appropriately reference sources below)
• Maps,plans,plots or plat submitted by or on behalf of the applicant/consultant: Wetland determination,Hemlock Scientific,9/26/2015
CI Data sheets prepared/submitted by or on behalf of the applicant/consultant.
Office concurs with data sheets/delineation report.
❑ Office does not concur with data sheets/delineation report.
❑ Data Sheet prepared by the Corps
❑ Corps navigable waters'study:
❑ USGS NHD Data.
❑ USGS 8 and 12 digit HUC maps.
❑ U.S.Geological Survey map(s)Cite quad name:
❑X USDA Natural Resources Conservation Service Soil Survey.Citation: unit 409,Deception-Disappear complex,10/26/2015
❑X National Wetlands Inventory map(s): IPF04B,Palustrine forested wetland,10/26/2015
❑ State/Local Wetland Inventory map(s):
❑ FEMA/FIRM map(s):
❑ 100-year Floodplain Elevation:
• Photographs:
❑X Aerial(Name&Date) Google Earth,10/26/2015
❑ Other(Name&Date)
❑ Previous determination(s).File#and date of response letter:
❑ Other Information:
Page 2 of 2
IMPORTANT NOTE:The information recorded on this form hal not necessarily been verified by the Corps and should not be relied upon
for Jater jurisdictional determinations.
•
•
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Zo t
Sign5tike and Date of Regulatory Project Manager Sig ature and Date of Person Reques g Preliminary JD
(REQ i RED) (REQUIRED,unless obtaining the signature is impracticable)
EXPLANATION OF PRELIMINARY AND APPROVED JURISDICTIONAL DETERMINATIONS: 1.The Corps of Engineers
believes that there may be jurisdictional waters of the United States on the subject site,and the permit applicant or other affected party who
requested this preliminary JD is hereby advised of his or her option to request and obtain an approved jurisdictional determination(JD)for that
site.Nevertheless,the permit applicant or other person who requested this preliminary JD has declined to exercise the option to obtain an
approved JD in this instance and at this time.2.In any circumstance where a permit applicant obtains an individual permit,or a Nationwide
General Permit(NWP)or other general permit verification requiring"preconstruction notification"(PCN),or requests verification for a non-
reporting NWP or other general permit,and the permit applicant has not requested an approved JO for the activity,the permit applicant is
hereby made aware of the toilowing:(l)the permit applicant has elected to seek a permit authorization based on a preliminary JO,which does
not make an official determination of jurisdictional waters;(2)that the applicant has the option to request an approved JD before accepting the
terms and conditions of the permit authorization,and that basing a permit authorization on an approved JO could possibly result in less
compensatory mitigation being required or different special conditions;(3)that the applicant has the right to request an individual permit
rather than accepting the terms and conditions of the NWP or other general permit authorization;(4)that the applicant can accept a permit
authorization and thereby agree to comply with all the terms and conditions of that permit,including whatever mitigation requirements the
Corps has determined to be necessary;(5)that undertaking any activity in reliance upon the subject permit authorization without requesting an
approved JD constitutes the applicant's acceptance of the use of the preliminary JO,but that either form of JD will be processed as soon as is
practicable;(6)accepting a permit authorization(e.g.,signing a proffered individual permit)or undertaking any activity in reliance on any
form of Corps permit authorization based on a preliminary JD constitutes agreement that all wetlands and other water bodies on the site
affected in any way by that activity are jurisdictional waters of the United States,and precludes any challenge to such jurisdiction in any
administrative or judicial compliance or enforcement action,or in any administrative appeal or in any Federal court;and(7)whether the
applicant elects to use either an approved JD or a preliminary JD,that JD will be processed as soon as is practicable.Further,an approved JD,
a proffered individual permit(and all terms and conditions contained therein),or individual permit denial can be administratively appealed
pursuant to 33 C.F.R.Part 331,and that in any administrative appeal,jurisdictional issues can be raised(see 33 C.F.R.331.5(a)(2)).If,during
that administrative appeal,it becomes necessary to make an official determination whether"CWA jurisdiction exists over a site,or to provide
an official delineation.of jurisdictional waters on the site,the Corps will provide an approved JD to accomplish that result,as soon as is
practicable.
•
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•
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, DEPARTMENT OF THE ARMY
M1) ALASKA DISTRICT,U.S.ARMY CORPS OF ENGINEERS
515. REGULATORY DIVISION
P.O.BOX 6898
JBER,ALASKA 99506-0898
Regulatory Division
POA-2015-545
Mr. Ryan Mathias
Post Office Box 110818
Anchorage, Alaska 99511
Dear Mr. Mathias:
This letter is in response to your September 28, 2015, request for a Department of
the Army (DA) jurisdictional determination for a parcel of land identified as
#05124309000. The property is located within Section 19, T. 15 N. R. 1 W., Seward
Meridian, USGS Map AK-ANCHORAGE B-7; at Latitude 61.3815° N., Longitude
149.5374°W.; Lot 4; Municipality of Anchorage, in Chugiak, Alaska. Your project has
been assigned number POA-2015-545, Fire Creek, which should be referred to in all
correspondence with us.
Based on our review of the information you provided and available to our office we
have preliminarily determined the subject property contains waters of the U.S., and/or
wetlands, under the Corps' regulatory jurisdiction. See the attached Preliminary
Jurisdictional Determination (PJD) Form. Please sign and return the form to our office.
A PJD is nct appealable. At any time you have the right to request and obtain an
Approved Jurisdictional Determination, which can be appealed. If it is your intent to
request an Approved JD, do not begin work until one is obtained.
Department of the Army authorization is required if you propose to place dredged
and/or fill material into waters of the U.S., including wetlands. You can find a copy of
the DA permit application online at www.poa.usace.army.mil/Missions/Regulatory.aspx.
You can refer to the sample drawing on our website at www.poa.usace.army.mil/
Portals/34/docs/regulatory/guidetodrawings2012.pdf.
Clean Water Act requires that a DA permit be obtained for the
Section 404 of the
placement or discharge of dredged and/or fill material into waters of the U.S., including
jurisdictional wetlands (33 U.S.C. 1344). The Corps defines wetlands as those areas
that are inundated or saturated by surface or groundwater at a frequency and duration
sufficient to support, and under normal circumstances do support, a prevalence of
vegetation typically adapted for life in saturated soil conditions.
-2-
Nothing in this letter excuses you from compliance with other Federal, State, or local
statutes, ordinances, or regulations.
If you have questions or to request a paper copy of the DA permit application,
please contact me via email at Julie.C.Ruth@usace.army.mil, by mail at the address
above, by phone at (907) 753-2735, or toll free from within Alaska at (800) 478-2712.
Sincerely,
1
Julie Ruth
Regulatory Specialist
Enclosures
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J. A. MUNTER CONSULTING, INC.
January 19, 2018
Mr. Ryan Mathias
Mathias Construction
P.O. Box 110818
Anchorage AK 99511
Re: Evaluation of aquifers in the vicinity of Birchwood Loop Subdivision, Anchorage,
Alaska.
Dear Mr. Birchwood Loop:
This letter report is to provide the findings of recent aquifer testing and evaluation of aquifer
conditions in the vicinity of the proposed Birchwood Loop Subdivision in the South Birchwood
area of Anchorage, Alaska. Birchwood Loop Subdivision has received preliminary plat approval
for 6 lots on approximately 18 acres. The purpose of the evaluation is to determine if there is
enough water to support on-site wells and to determine whether any surrounding well owners
would be adversely affected.
Hydrogeologic Setting
A detailed geologic map of the area by Yehle and Schmoll (1987) shows that the predominant
surficial geologic unit at the site is comprised of glacial deposits from the Elmendorf glaciation.
The deposits are primarily ground moraine with some kame deposits. The ground moraine
deposits are "chiefly diamicton consisting of massive, unsorted to poorly sorted mixtures of
gravel, sand, silt,and some clay; includes scattered boulders". The kame deposits are chiefly
sand and gravel. Moraine-derived colluvium and minor alluvial deposits associated with a small
stream flowing through the site are also present. The Elmendorf glaciation is the youngest of the
Quaternary glaciations in this part of Cook Inlet. The regional hydrogeology is described by
Kikuchi (2013)who's study area included a large portion of the Matanuska Susitna Borough
directly across Knik Arm from this site and only a few miles away. The surficial sediments in
the vicinity of Birchwood Loop Subdivision are up to a few tens of feet thick and in general do
not constitute a viable source of water to wells. No nearby wells are known to tap these deposits
for water supply.
Unconsolidated deposits in the area are underlain by Tertiary-age bedrock units of the Kenai
Group consisting of interbedded layers of, sandstone, siltstone,claystone, and minor coal. Most
or all wells in the general vicinity tap these bedrock units for water supplies.
METHODS AND SOURCES OF DATA
This report provides a vicinity analysis that includes an evaluation of well data from surrounding
properties to evaluate the general conditions in the area. Groundwater recharge information is
reviewed to estimate potential sustainable aquifer yields. Test well drilling and aquifer testing
was conducted to determine the properties of aquifers present at the site. Aquifer test data were
5701 PENNY CIRCLE,ANCHORAGE,AK,99516
jamunter cr arctic.net
PHONE(907)345-0165; FAX(907)348-8592
J. A. MUNTER CONSULTING, INC.
analyzed using software by AQTESOLV Pro 4.0. The aquifer characteristics are used to model
expected responses in wells from the proposed new pumping and assess the water-supply
potential at the proposed Birchwood Loop Subdivision and the potential impacts of the
development on surrounding properties.
VICINITY ANALYSIS
Aquifer Recharge and Water-Supply Potential
The bedrock aquifer in this area receives recharge through the overlying glacial deposits. These
deposits commonly have a water table perched on top of the bedrock surface that slowly leaks
water into the near-surface fractures of the aquifer.
Kikuchi (2013, Figure 12)estimates that groundwater recharge across Knik Arm from this site
averages 1.5 to 5.8 inches per year across a broad area. A conservative estimate is that
groundwater recharge at Matthias Subdivision averages approximately 3 to 4 inches per year.
This translates to an average of approximately 670 to 890 gallons per day being recharged on
each of the six planned lots on the parcel. This amount of water is considerably more than the
Municipal requirement of 450 gpd for a 3-bedroom home. In addition to direct recharge of water
onto lots, however,this subdivision also is likely to receive groundwater inflow from upgradient
areas. In general, groundwater flows from the Chugach Mountain front to Knik Arm through
this area. These data suggest that the potential supply of water is sufficient to sustain aquifers
with the quantity of water needed for use by well owners both within the proposed subdivision
and also in surrounding developments.
Review of Area Well Records
The MOA's On-site files were searched for records from adjacent and surrounding properties
(http://onsite.ci.anchorage.ak.us/WebLink/Browse.aspx?startid=l). The WELTS well log
database (http://www.navmaps.alaska.gov/welts/) maintained by the ADNR was also examined
for well logs. Tables 1 presents the results of the data search. Twelve well logs were identified.
Following is a table of key data elements from well logs in the vicinity of the proposed
development. Transmissivities (T) were estimated using the formula: T=2000 x specific
capacity,where specific capacity=reported yield/drawdown (Sterrett, 2007,Appendix 6.N).
Full drawdown is assumed where data were lacking, resulting in conservative (i.e. low) estimates
of T.
Table 1. Summary of data for wells near Birchwood Loop Subdivision.
Location Well Reported yield or Estimated Aquifer Static water level in
depth flow rate and year of transmis- type feet below land surface
(feet) measurement(gpm) sivity and year of
(gpd/ft) measurement
L2,3,4, Trct 303 1.8 1984 60 Bedrock 103 1984
B Birch
Woods
Evaluation of aquifers in the vicinity of Page 2 of 9 January 19,2018
Birchwood Loop Subdivision, Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
Location Well Reported yield or Estimated Aquifer Static water level in
depth flow rate and year of transmis- type feet below land surface
(feet) measurement(gpm) sivity and year of
(gpd/ft) measurement
L24 T15N 94+ 1.1 2005 35 unknown 32 2005
R1 W Sec 19
L205A 7 1986 311 30 1986
T15N R1 W 75 2.2+ 2012 66+ Bedrock 8 2012
Sec 18
L2,Thibault 5 1984 170 42 1984
102 5.2 2013 160 Bedrock 36 2013
L42A Travis unkno 0.7 2010 Not unknown 41.4 2010
Estates wn calculable
L42B Travis 265 5 1983 49 Bedrock 60 1983
Estates
L23 T15N 111 8 1973 176 20 1973
R1 W Sec 19 1.5 2010 36 Bedrock 27.8 2010
L41 T15N 1 2009 27 126 2009
R1 W Sec 19 200 0.70 2014 16 Bedrock 112 2014
L203 T15N 3 1978 41 55 1978
R 1 W Sec 18 200 0.64+ 2005 8+ Bedrock 42 2005
0.97 2009 12 41 2009
Trct A Birch 2 1983 17 flows 1983
Woods Sub. 240 0.5 1987 4.5 Bedrock 19 1987
L2 Kahn 210 1.5 1986 15 4 1986
Subd. 0.64 2012 7 Bedrock 29 2012
Tract A 140 3.5 1987 51 4 1987
Birch 1.6 1990 24 Bedrock 4 1990
Woods Sub. 1.5 2003 22 4 2003
2.5 2007 37 <4 2007
Note: Estimated transmissivity (T) in gallons/day/ft calculated by T= SC x 2000 where SC
(specific capacity)=yield(in gpm)/drawdown(in ft).
Summary of Well Record Review
Ten wells in the vicinity were found to tap the bedrock aquifer and two other wells likely tap the
bedrock aquifer however those data are not reported. No wells are known to tap a sand and
gravel alluvial or glacial aquifer. Reported yields range from 0.5 to 8 gpm, and inspection of
water-level data collected during different years shows that water levels in the aquifer have
remained relatively stable. Using the most recent well-yield data for each well,the median
reported well yield is between 1.1 and 1.5 gpm.
Reported static water levels range in depth from approximately land surface to 126 ft below land
surface. Well depths range from 75 ft to 265 ft below land surface, with a median well depth of
200 ft. Calculated transmissivity values range from 4.5 to 311 gpd/ft. Using the lowest
Evaluation of aquifers in the vicinity of Page 3 of 9 January 19,2018
Birchwood Loop Subdivision,Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
reported value of transmissivity for each well,the median value of transmissivity is 35 gpd/ft.
This value is within the range for a fractured sandstone aquifer(Freeze and Cherry, 1979, p. 29).
The available well data indicate that wells in the vicinity are capable of supplying sufficient
water to single family homes on an on-going basis. While well yields from bedrock wells in this
area are low,they are generally adequate for household use. Some wells may benefit from in-
home water storage or well-deepening or hydrofracking to increase yields.
Dearborn and Barnwell (1975) observe that effective solutions to marginal well yields in bedrock
wells include deepening well bores to provide additional water storage within the well bore or
adding water storage in the home. Deepening the well may also increase the well yield by
tapping previously untapped fractures. Another potential solution to increase yield from the
aquifer is to move to another location on the lot and drill a new well.
Wells that exhibit declining yields over time should be evaluated by a well professional for
plugging. Plugging can be caused by sediment accumulations, iron hydroxide bioaccumulations,
or precipitated calcium carbonate, all of which can occur in wells subject to large fluctuations in
water levels caused by normal water usage. All of these plugging problems can be treated by
commonly available physical or chemical treatment methodologies.
Summary of Vicinity Analysis. The proposed subdivision is located in an area where numerous
wells already tap the bedrock aquifer. Existing data show that the aquifer is not exhibiting
water-level declines from existing development and thus the aquifer appears not to be
significantly stressed by existing development. Local aquifer recharge studies suggest that the
aquifer has the potential to supply the water required for indefinite sustainable on-site use for the
proposed Birchwood Loop Subdivision.
SITE EVALUATION
Test-Well Drilling
Two test wells were drilled on lots 4 and 5 as shown on the attached Figure from Garness
Engineering, Group,Ltd (12/13/17 - Revised). Logs of the wells are contained in the
Attachments. There is a pre-existing well on Lot 3 of the proposed subdivision for which no log
is available, however an inspection revealed that the well is 340 feet deep. For this report, the
well located on Lot 3 (340 ft deep) will be called Well 3, the well located on Lot 4 (82 ft deep)
will be called Well 4,and the well located on Lot 5 (262 ft deep) will be called Well 5. All of
the wells tap the bedrock aquifer.
Aquifer Testing Results
Testing of Well 3. Before Wells 4 and 5 were drilled, Well 3 was test pumped for 24 hours
(Wheaton Water Well, Inc. flow test results, attached). The well is a relatively low-yield well,
and upon pumping at a rate of several gallons per minute,the water level was drawn down to the
pump intake. The well was intermittently pumped and allowed to recover for the remained of
the 24-hour test period. A totalizing meter showed that the well produced 1426 gallons of water,
Evaluation of aquifers in the vicinity of Page 4 of 9 January 19,2018
Birchwood Loop Subdivision,Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
for an average of 0.99 gpm for the 24-hour period. Using the methods described in Table 1 to
estimate transmissivity,the estimated aquifer transmissivity at Well 3 is 12 gpd/ft,which is
within the range of values of surrounding wells shown in Table 1.
Testing of Well 4. After Wells 4 and 5 were drilled, Well 4 was pumped for 24 hours on Dec.
19-20, 2017, while monitoring water levels in Wells 3 and 5. The well was pumped at a constant
rate of 17 gpm, which was the maximum flow rate of the pump. The pumped well drew down a
total of 18.35 feet, Well 3 drew down a total of 0.05 feet and Well 5 drew down a total of 0.5 feet
during the test(Wheaton Water Well, Inc. Well Flow Test, 12-19-2017 -see attached). The
minimal drawdown observed in Wells 3 and 5 indicated that they mostly tap different fracture
systems in the bedrock aquifer and that they are not suitable for typical aquifer test analysis for
aquifer parameters transmissivity and storativity from this test.
The drawdown data and aquifer analysis based on data collected in the pumped well using
software Aqtesolv Pro 4.0 are shown in an attachment. The calculated transmissivity of the
aquifer is 282 ft2/day,or 2,110 gpd/ft. This is significantly higher than all of the calculated
transmissivity values from surrounding wells (Table 1), indicated that this well tapped into an
unusually productive portion of the bedrock aquifer.
Storativity of the aquifer could not be calculated with the drawdown data from only the
production well. A responding observation well is required to calculate valid values of
storativity.
The testing deviated from one of the aquifer test guidelines provided by the Municipality of
Anchorage. This guideline calls for achieving 70 percent of available drawdown at the end of
the test. Drawdown at the end of the test was only about 30%of available drawdown. This is
considered only a minor and inconsequential deviation from the guidance that is not expected to
have any significant effect on test results or the conclusions of this report for the following
reasons:
1. The calculation for transmissivity of the aquifer at the site of Well 4 are not likely to change
significantly even if a higher pumping rate would have been used and more drawdown would
have occurred. The mathematics of the Theis(1935) solution apply equally to any pumping rate.
Commonly-cited references such as ASTM Standard D 4043-96 (Reapproved in 2004) and
Sterrett(2007)make no mention of establishing an arbitrary amount of drawdown that needs to
be achieved in order for a test to be considered valid. This may be a result of the difficulty of
determining in advance the constant flow rate needed to achieve a certain amount of drawdown.
In this case,the creation of more than 18 feet of drawdown over a 24-hr period shows that the
aquifer was stressed sufficiently to make a reasonable calculation of transmissivity using
commonly accepted methods. The value of transmissivity determined is well within the ranges
of other transmissivities determined or cited during this investigation for this vicinity and is
considered valid for the purposes of this report.
2. The well test yielded more water than expected with less drawdown. Based on previous
drilling and testing results in the vicinity (see Table 1), this well was not expected to yield so
much water. The finding of"more water than expected" illustrates the natural variability of a
Evaluation of aquifers in the vicinity of Page 5 of 9 January 19,2018
Birchwood Loop Subdivision,Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
fractured bedrock aquifer of this type and the difficulty of predicting a well's response to
pumping in advance.
3. The conclusions of the report are more dependent on the assessment of the lower end of the
range of water availability, or threshold values,than the upper end, so that refinement of estimate
of the aquifer transmissivity would not have a major impact on the subsequent assessment of the
potential effects of new pumping at the site.
4. The overall testing program for the aquifer at this site is quite rigorous, even with the
deviation from the guideline described above. The guidelines allow for the completion of only
one 24-hr test if the observation wells respond to pumping from the first well tested. The
completion of three 24-hr tests provides assurance that the overall results are representative of
the site and that the analysis of the effects of pumping from new wells is founded on sound data.
Well 5 Testing. Aquifer testing was next performed using Well 5 as the pumped well and Wells
3 and 4 as observation wells. The test was initiated on January 3, 2018 at a flow rate of 2 gpm.
the flow rate was reduced to 1.5 gpm after 270 minutes of pumping and was further reduced to 1
gpm after 287 minutes of pumping. Pumping continued at 1 gpm for the remainder of the test
(Wheaton Water Well, Inc. Well Flow Test, 1-3-2018 - see attached). The drawdown data and
aquifer analysis based on data collected in the pumped well using software Aqtesolv Pro 4.0 are
shown in an attachment. The calculated transmissivity of the aquifer is 0.35 ft2/day,or 2.6
gpd/ft. This is just below the low end of the range of transmissivity values from surrounding
wells (Table 1).
There were no identifiable water-level changes in the monitoring wells in response to the
pumping.
Summary of Site Evaluation
Test drilling and aquifer testing at Birchwood Loop Subdivision yielded estimates of
transmissivity of 2.6, 12, and 2,110 gpm/ft from three separate 24-hr aquifer tests at three
different wells. These data are similar to the range of values determined from the vicinity
analysis, except that Well 4 yielded a significantly higher transmissivity value. It was not
possible to estimate aquifer storativity from the test data. No significant water-level responses to
pumping were noted in observation wells during any of the tests, suggesting that the fracture
zones tapped by the wells were not closely interconnected.
POTENTIAL EFFECTS OF NEW PUMPING
An analysis of the effects of pumping new wells both on future neighboring wells within
Birchwood Loop Subdivision and also on surrounding wells is described below using the method
of Theis(1935). The Theis(1935) method requires certain simplifying assumptions. It is
assumed that the aquifers are infinite in lateral extent without boundary conditions, are
homogeneous and isotropic, and that recharge does not occur within the simulation time period.
While these assumptions are simplifications of actual aquifer conditions,the Theis(1935)model
Evaluation of aquifers in the vicinity of Page 6 of 9 January 19,2018
Birchwood Loop Subdivision,Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
is widely used and can provide an initial assessment of the magnitude of the likely effects of
pumping on nearby wells.
This aquifer analysis assumes that all the wells for this analysis tap the same bedrock aquifer
with a transmissivity of 40 ft2/day, which is the geometric mean of the three test well
transmissivities. This assumed value is very close to the median calculated transmissivity for
surrounding wells,which is 35 gpd/ft(Table 1). The value assumed for aquifer storativity for the
model simulations is 0.001. This value intermediate between values typical of a fully confined
aquifer and values typical of a fractured-rock water-table aquifer. This value assumes that a
small amount of water would likely be available from dewatering fractures in the upper part of
the aquifer during pumping.
Pumping is assumed to occur for 200 days, which is the approximate duration of wintertime
conditions with no or minimal recharge,after which recharge would supply additional water to
the aquifer.
First, drawdown at a closely spaced well pair is considered. The closest-spaced well pair is on
Lots 1 and 2 of the proposed Birchwood Loop Subdivision, where the wells would be 20 feet
apart (see Figure). Pumping one well for 200 days at a rate of 450 gpd results in calculated
drawdown at the other well of 7.8 feet. Review of the well data in Table 1 shows that this is
much less than the expected available drawdown in future wells at the site. Thus,the effects of
future pumping on neighboring individual wells within the subdivision is concluded to be
insignificant. This is consistent with the results of aquifer testing at Wells 4 and 5 showing
minimal or nonexistent well interference in neighboring wells.
Next,the neighborhood analysis was conducted by examining the effects of cumulative pumping
from all six proposed new wells on neighboring wells. The attached Figure shows that
neighboring wells are approximately 300 feet or more from the geographic center of the
proposed subdivision.
After simulated pumping for 200 days at a total rate of 2700 gpd(450 gpd/lot times 6 lots), 17.8
feet of drawdown is calculated at a distance of 300 feet from the center of pumping.
Examination of the well data shown in Table 1 shows that the available drawdown in
surrounding wells is far greater than this amount of drawdown, ranging from approximately 60
to more than 200 feet. Thus,the projected drawdown would be only a small portion of the
available drawdown and it is concluded that the effects of the proposed pumping on surrounding
wells would be minor and that surrounding wells would be able to continue producing water
under these circumstances. These calculations contain numerous conservative assumptions and
the actual impacts of the development of Birchwood Loop Subdivision are expected to be less
than those described above.
SUMMARY AND CONCLUSIONS
All wells in the Birchwood Loop Subdivision are likely to tap a bedrock aquifer. Separate
testing of three test wells shows bedrock aquifer characteristics similar to wells in the vicinity,
although one of the wells was more productive than any surrounding wells. All wells tested are
Evaluation of aquifers in the vicinity of Page 7 of 9 January 19,2018
Birchwood Loop Subdivision,Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
adequate to meet Municipality of Anchorage requirements for single family domestic usage and
analysis of wells in the vicinity indicates that future drilled wells on the parcel are also highly
likely to be adequate for single family domestic usage. Future wells drilled on the property,
however, could produce less than 1 gpm and benefit from yield enhancement through deepening
or hydrofracking or in-home supplemental water storage to meet peak demands.
Monitoring of the wells showed minimal well interference between the wells, suggesting that the
wells tested tap fracture systems in the bedrock aquifer that are substantially separate.
Historic water-level declines are not evident in the bedrock aquifer and the local hydrologic
regime appears to be adequate to support existing and new water demands from wells as
proposed.
Model calculations indicate that up to approximately 18 ft of drawdown is possible at the closest
surrounding wells. These calculations suggest that some amount of water level response will
occur in surrounding wells as a result of pumping from new wells at Birchwood Loop
Subdivision. A review of well logs shows that wells in the vicinity have adequate available
drawdown, indicating that such water-level declines would not adversely affect the performance
of those wells.
The multiple lines of analysis conducted for this evaluation all provide consistent support to the
findings that there is an adequate supply of water for on-site wells to support the proposed
Birchwood Loop Subdivision and that the new use of water will not adversely affect the ability
of surrounding water users to obtain water.
CLOSING
Should you have any questions about this report,please feel free to call me at 345-0165 or 727-
6310.
Sincerely,
J. A. Munter Consulting, Inc.
laCt...4--Q-4 a
--p6_,___L____,
James A. Munter, CPG, CGWP
Principal Hydrogeologist
Certified Ground Water Professional No. 119481
Alaska Licensed Professional Geologist No. 568
Attachments:
Figure
Well Logs, Wells 4 and 5
Wheaton Water Well, Inc., Flow test results,Anchorage Parcel # 051-243-09
Wheaton Water Well, Inc. Well Flow Test data, 12-19-2017
Evaluation of aquifers in the vicinity of Page 8 of 9 January 19,20 18
Birchwood Loop Subdivision,Anchorage,Alaska
J. A. MUNTER CONSULTING, INC.
Wheaton Water Well, Inc. Well Flow Test data, 1-3-2018
AQTESOLV Flow Test Well 4 Results
AQTESOLV Flow Test Well 5 Results
References Cited
ASTM, 2004, Standard guide for selection of aquifer test method in determining
hydraulic properties by well techniques, ASTM Designation D 4043 — 96 (reapproved 2004),
ASTM, 100 Barr Harbor Drive, Conshohocken PA. 6 p.
Dearborn, L. L., and W. W. Barnwell, 1975, Hydrology for Land-use Planning, the
Hillside area, Anchorage, Alaska, U.S. Geological Survey Open-file report 75-105.
Freeze R. A., and J. A. Cherry, 1979, Groundwater, Prentice Hall, Englewood Cliffs, NJ,
604 p.
Kikuchi, Colin P., 2013, Shallow Groundwater in the Matanuska-Susitna Valley, Alaska-
Conceptualization and Simulation of Flow. U.S. Geological Survey Scientific Investigations
Report 2013-5049.
Papadopulos, I. S. and H. H. Cooper, 1967. Drawdown in a well of large diameter, Water
Resources Research, vol. 3, no. 1,pp. 241-244.
Sterrett, Robert J., ed., 2007, Groundwater and wells, 3`a edition, Johnson Screens, A
Weatherford Company,New Brighton, Minnesota, 812 p. plus appendices.
Theis, C. V., 1935, The relation between the lowering of the piezometric surface and the
rate and duration of discharge of a well using groundwater storage. Trans. Amer. Geophys.
Union, 2,pp 519-524.
Yehle, L. A, and H. R. Schmoll, 1987, Surficial geologic map of the Anchorage B-7 NW
quadrangle, Alaska, U. S. Geological Survey Open-File Report 87-168.
Evaluation of aquifers in the vicinity of Page 9 of 9 January 19,2018
Birchwood Loop Subdivision,Anchorage,Alaska
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LOCATIONS ARE SHOWN BASED UPON D.O.S 4 / �.._i
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Wheaton Water Well, Inc.
1190 N. Wasilla-Fishhook Road
Wasilla, AK 99654
(907)376-2041
I
Name: Ryan Mathias
Address: 13120 Lupine Road
City: Anchorage State: AK Zip Code: 99516
Well Site: T15N, R1 W, S19 Lot: 4 Block:
Additional: Permit# OSP171363
Well Depth: 82 ft. From: To: Formation:
0 14 fill
Below Ground: 80 ft. 14 16 wood(pine)
Above Ground: 3 ft. 16 17 topsoil
Gal/Min: 10 17 23 wet silty gravel
Static Level: 15 ft. 23 30 silt
50'of 6" ID Steel 30 47 hard packed silt,sand
Casing: 47 48 coal
Liner Pipe: 40 ft. 48 66 soft gray rock
Screened: none 66 67 coal
Perforated: none
67 82 soft gray rock
Grouted: Bentonite
Depth: 20'+ water is coming from 43 ft.to
45 ft. and 50 ft.to 51 ft.
Develop. Method: These measurements are from
Use of Well: Residential the top of the casing.
Drilling Method: Rotary
Misc.: Well disinfected with
Liner pipe is set from 42 ft.
Misc: chlorine 50 ppm to 82 ft. and perforated.
Other: none
'Date Drilled: 12-13-2017 Driller: Seth Moore 1
Wheaton Water Well, Inc.
1190 N. Wasilla-Fishhook Road
Wasilla, AK 99654
(907)376-2041
Name: Ryan Mathias
Address: 13120 Lupine Road
City: Anchorage State: AK Zip Code: 99516
Well Site: T15N, R1 W, S19 Lot: 5 Block:
Additional: Permit# OSP171369
Well Depth: 262 ft. From: To: Formation:
Below Ground: 260 ft. 0 9 silt,gravel
Above Ground: 2 ft• 9 12 wood/muck,silt
12 17 topsoil
Gal/Min: 2 17 41 silt,gravel
Static Level: top of casing 41 44 hard packed sand, silt
Casing:
46' of 6"ID Steel 44 67 sandstone
67 68 coal
Liner Pipe: 220 ft. 68 83 sandstone
Screened: none 83 84 coal
Perforated: none
84 94 sandstone
94 98 damp sandstone(1 gpm)
Grouted: Bentonite 98 167 sandstone
Depth: 20'+ 167 196 soft brown shale(1 gpm)
Develop. Method: Air 196 262 sandstone
Use of Well: Residential
Drilling Method: Rotary
Misc.: Well disinfected with
Liner pipe is set from 42 ft.
Misc: chlorine 50 ppm to 262 ft. and perforated.
Other: none
Pate Drilled: 12-15-2017 Driller: Ben Mattson
Wheaton Water Well, Inc.
907-376-2041 -Fax:907-376-2030-email:brianw!dwheatonwells.com
1190 N. Wasilla-Fishhook Road
Wasilla, AK 99654
To Whom It May Concern:
On October 10,2017 a 24 hour flow test was performed at the following property:
17620 S. Birchwood Loop Road
T18\, R1 W, 519, Lot 4REM
Anchorage Parcel if:051-243-09
The well is approximately 340 feet deep with 90 feet of casing. A pump was installed
and encountered an obstruction at 188 feet. The pump intake was set at 170 feet. The
test was performed using low water protection. A total of 1,426.09 gallons of water was
pumped in the 24 hour period. It was determined that the well is producing.99 gpm.
Wheaton Water Well, Inc.
1190 N. Wasilla-Fishhook Road
Wasilla,AK 99654
(907)376-2041
WELL FLOW TEST
Project: Ryan Mathias Date of Test: 12-19-2017
Well Site: T15N,R 1 W, S19 Lot 4 Casing: 50' of 6"ID Steel
Well Depth: 82' Liner Pipe: 40 ft.
Static Water Level: 15 ft. Date Level Taken: 12-13-2017
Date Drilled: 12-13-2017 Drilled By: Wheaton Water Wells
Time Gallons Per Static Draw Down Draw Down Remarks
Minute Level Well#3 Well#5
11:15 am 0 14.01' 21.75' 5.60' Start Pumping
11:16 17 20.49'
11:17 17 23.90'
11:18 17 24.72'
11:19 17 25.28'
11:20 17 25.89'
11:21 17 26.41'
11:22 17 26.70'
11:23 17 27.02'
11:24 17 27.11'
11:25 17 27.22'
11:26 17 27.33'
11:31 17 27.78'
11:36 17 28.06'
11:41 17 28.28' 21.75' 5.60'
11:46 17 28.47'
11:51 17 28.63'
11:56 17 28.78'
12:01 pm 17 28.91'
12:06 17 29.02'
12:11 17 29.12'
12:16 17 29.18'
12:21 17 29.27'
12:26 17 29.38'
Page 1 of 3
Time Gallons Per Static Draw Down Draw Down Remarks
Minute Level Well#3 Well#5
12:31 17 29.43'
12:41 17 29.59'
12:51 17 29.65'
1:01 17 29.76'
1:11 17 29.83'
1:21 17 29.88'
1:31 17 29.94'
1:41 17 30.01'
1:51 17 30.08'
2:01 17 30.08'
2:11 17 30.14'
2:21 17 30.18'
2:31 17 30.22'
2:41 17 30.26'
2:51 17 30.32'
3:01 17 30.38'
3:11 17 30.43' 21.75' 5.81'
3:21 17 30.47'
3:41 17 30.53'
4:01 17 30.61'
4:21 17 30.65'
4:41 17 30.74'
7:37 17 31.09' 6.08'
8:25 17 31.23'
10:29 17 31.67'
12:00 am 17 31.98'
12:32 17 32.11'
3:00 17 32.16'
6:00 17 31.95'
9:37 17 31.40'
10:27 17 32.36'
11:16 17 32.15' 21.80' 6.10' Stop Pumping
Page 2 of 3
RECOVERY
Time Static Draw Down Draw Down Remarks
Level Well#3 Well#5
11:18 am 27.60'
11:19 24.10'
11:20 22.50'
11:21 19.30'
11:22 19.00'
11:23 18.80'
11:24 18.70'
11:25 18.68'
11:26 18.64'
11:27 18.59'
11:32 18.41'
11:33 18.38'
11:34 18.35'
11:35 18.33'
11:36 18.31'
11:37 18.29'
11:38 18.26'
11:39 18.24'
11:40 18.23'
11:41 18.22'
12:32 pm 17.36'
12:35 21.77'
12:39 6.12'
Page 3 of 3
Wheaton Water Well, Inc.
1190 N. Wasilla-Fishhook Road
Wasilla,AK 99654
(907)376-2041
WELL FLOW TEST
Project: Ryan Mathias Date of Test: 1-3-2018
Well Site: T15N, R1W, S19 Lot 5 Casing: 46' of 6"ID Steel
Well Depth: 262' Liner Pipe: 220 ft.
Static Water Level: Top of Casing Date Level Taken: 12-15-2017
Date Drilled: 12-15-2017 Drilled By: Wheaton Water Wells
Time Gallons Per Static Draw Down Draw Down Remarks
Minute Level Well#4 Well #3
10:44am 0 15.25' 13.90' 21.85' Start Pumping
10:45 2.4 17.40' Pump Intake is at 244'
10:46 2.3 18.60'
10:47 2.2 19.90'
10:48 2.1 22.21'
10:49 2.0 23.39'
10:51 2.0 26.72'
10:52 2.0 27.90'
10:53 2.0 28.98'
10:54 2.0 29.99'
10:55 2.0 31.10'
11:00 2.0 36.90'
11:05 2.0 42.50'
11:10 2.0 48.90'
11:15 2.0 54.80'
11:25 2.0 65.90'
11:35 2.0 76.40'
11:45 2.0 86.00'
12:00 pm 2.0 98.80' 13.90' 21.87'
12:15 2.0 110..80'
12:30 2.0 122.40'
Page 1 of 3
Time Gallons Per Static Draw Down Draw Down Remarks
Minute Level Well#4 Well#3
1:00 2.0 143.40' 13.90' 21.90'
1:30 2.0 163.80'
2:00 2.0 184.50'
3:00 2.0 221.50' 13.90' 21.88'
3:15 1.5 233.90' Throttle down flow rate
3:25 1.5 234.50'
3:30 1.5 237.81'
3:34 1 Throttle down flow rate
3:37 1 240.80'
3:42 1 240.50'
3:47 1 240.30'
3:52 1 240.10'
4:02 1 239.50'
4:12 1 238.90'
4:42 1 237.70'
5:12 1 237.50'
6:12 .8 227.10'
6:36 1 228.30'
7:12 1 228.95'
8:12 1 229.51'
9:14 1 229.45' 13.92' 21.87'
10:16 1 233.81'
10:28 1 234.39'
10:38 1 234.79'
10:52 1 235.43'
11:02 1 235.60'
11:18 1 236.16'
11:28 1 236.40'
11:48 1 236.91'
12:08 am 1 237.79' 13.91' 21.88'
12:28 1 238.45'
12:50 1 238.52'
2:06 1 238.39' 13.92' 2L87'
5:09 1 239.21' 13.91' 21.87'
7:08 1 239.86' 13.91' 21.86'
10:40 1 242.21' 13.91' 21.91'
11:00 1 242.33'
11:05 1 242.32' Stopped Pumping
Page 2 of 3
RECOVERY
Time Static Draw Down Draw Down Remarks
Level Well#4 Well#3
11:05 am 242.32' Stopped Pumping
11:06 236.14' Check valves failed due to
11:07 232.44' sediment in the water.
11:08 229.95'
11:09 228.44'
11:10 227.38'
11:11 226.41'
11:12 225.82'
11:13 225.15'
11:14 224.50'
11:15 223.82'
11:20 220.53'
11:25 217.34'
11:30 213.75'
11:35 210.21'
11:45 204.19'
11:55 197.42'
12:05 pm 191.16'
12:10 188.27' 13.91'
12:18 21.89'
12:30 173.52'
12:40 167.52'
12:50 161.71'
1:30 140.53'
2:00 127.24'
2:30 115.65'
3:00 105.43'
3:30 96.82'
4:00 89.21'
4:30 83.10'
5:00 77.80'
6:00 68.12'
7:00 61.12'
8:00 55.62'
9:00 50.95'
10:00 47.02'
Page 3 of 3
1111111.1111111
100. 1 1 1 1 ; 1 !r1 1 I 1 1 1 1 I11 1 1 1 1 Intl 1 1 1 1 1 111
D
s - -
p
I _ -
a
m 10. — -'
e - -
n - -
t -
f
t
1. 111.1 1 1 1 1 II -!.__ I. I 1 1 1 111
1. 10. 100. 1000. 1.0E+4
Time (min)
FLOW TEST WELL 4
Data Set:
Date: 01/11/18 Time: 15:31:54
PROJECT INFORMATION
Company: J A Munter Consulting Inc
Client: Mathias Subdivision
Location: Lot 4
Test Well: Well 4
Test Date: 12/19-20/17
WELL DATA
Pumpinr Wells Observation Wells
Well Name X(ft) Y(ft) (Well Name X Oft) Y Oft)
Well 4 0 0a
SOLUTION
Aquifer Model: Confined Solution Method: Theis
T =281.7 ft2/day S = 1.753E-6
KzlKr= 1.
b = 35_ft
300. i- . . Ir , I 1 I i , tiiil I I I lith/ , , r 11111
D 240. —
i
P n
O o
O O
n a
X180. — 0 G —
e0 col
O O
m 0 o
- h a,
0
0
t 120. _ ob n _
- fl
dh-
( O
f °
t 60. — na
o
o -
-
0. --t---1 QiiIIl I 1 1 11111 1 1.111L1_ - 1 Ili
1. 10. 100. 1000. 1.0E+4
Time (min)
FLOW TEST WELL 5
Data Set: C:\...\flow test 5.aqt
Date: 01/11/18 Time: 16:55:54
PROJECT INFORMATION
Company: J A Munter Consulting Inc
Client: Mathias Subdivision
Location: Lot 5
Test Well: Well 5
Test Date: 1/3-4/18
AQUIFER DATA
Saturated Thickness: 218. ft Anisotropy Ratio (Kz/Kr): 1. -
WELL DATA
PumpingWells Observation Wells
LWell Name
X(ft) Y(ft) I o Well 5 Well Name X(ft) -Y(ft)
Well 5 0 0
SOLUTION
Aquifer Model: Confined Solution Method: Papadopulos-Cooper
T = 0.3497 ft2/day S = 0.003666
r(w) = 1.ft r(c) = 0.25 ft